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Structural Fill: Structural fill continued to be hauled to the PSSA toe berm area widening the haul road, using <br />several Cat 777 and several 740 haul trucks. The structural fill material was placed in an approximately 18 to 24 <br />inch loose lifts by a John Deere 1050J and D1 OR dozers followed by a Cat CS56B vibratory, 10 -ton, smooth-drum <br />roller that compacted the placed materials with a minimum of four passes (By method specification). <br />In addition to the structural fill placement for the PSSA toe berm embankment, the contractor continued cut to fill <br />operations and compaction by method specification located at the mid -way ADR haul road location at approximate <br />Sta.50 +00 — 53 +00. A Cat D8 Dozer with GPS and a Cat C556 Smooth Drum roller was utilized. Progress is <br />expected to continue. <br />See Hwy 67 below for detail of embankment fill progress. <br />Note: An Amec field representative monitored structural fill material temperatures placed within the areas of fill <br />during all shifts. Average structural fill temperatures were above 32 °F <br />Clay (SLF) Processing: <br />Cameron Site: No clay mining or processing occurred during this reporting period due to a saturated site from <br />previous rains. <br />Squaw Gulch Site: <br />No work occurred at the VLF clay borrow site during this reporting period. <br />Underdrain System: <br />Secondary Underdrain: No work was performed on the Secondary underdrain during this reporting period. <br />A total of 1380 feet of Secondary underdrain has been completed. <br />Primary Underdrain: No work was performed on the Primary underdrain during this reporting period. <br />A total of 1280 feet of Primary underdrain has been completed. <br />Temporary Underdrain: Temporary underdrain pipe is installed thru the embankment. No other work occurred <br />during this reporting period. <br />Tree /Slash Clearing, Chipping: <br />Seed Masters paused operations until further notice. <br />B) Underground Workings <br />Confirmatory drilling was performed on underground working No. 6132, No. 6187, No. 6239 during this reporting <br />period. All drill hole locations were established on a 4 -foot center isolating any voids found. Further remediation <br />efforts will be ongoing until remediated. Summary of the remediation efforts will follow 100% remediation. <br />During this reporting period exploratory excavation was performed on UG working No. 6202 and No. 6203. Site's <br />listed require further investigation and excavation into bedrock as remediation continues to be completed. <br />During this reporting period remediation efforts were performed and completed on UG working No.6122, No. 6194, <br />No. 6195, No. 6203 and No. U6263. Sites listed were excavated to practical refusal into rock varying depths <br />depending on the working remediated. The site for each working was then backfilled in 2 foot loose lifts to <br />approximate planned subgrade elevation using the onske structural fill (excavated material) and "bucket tamped" <br />with the back of the CAT 330 excavator bucket. All backfill material was free of organic material, ice and snow and <br />are considered remediated as specified. <br />Page 2 of 6 MLE2 WE 08.10.13.doc <br />