Laserfiche WebLink
<br />r~(- <br />"''";.;. <br />OPERATION AND MAINTENANCE <br /> <br />"3') <br /> <br />stop leakage, A worn shaft coupling in the No, 1 flocculator was <br />repaired, The sump in the lower sludge basin was rebuilt to elimi- <br />nate plugging of the sludge line and to permit the line to carry the <br />full load when both sludge pumps are in operation, During the <br />6-day Rhutdown in March, the first opportunity presented itself <br />for detailed inspection of many parts of the plant which were in- <br />accessible during operation when all the channels were full of <br />water, The main influent and effluent channels were cleaned of <br />accumulated sludge, The holes in the carbon dioxide diffusers in <br />the zeolite influent channel were reamed. All the valves in the filter <br />influent and effluent channels and in the zeolite influent channel <br />were inspected. In general, the facilities were found to be in excel- <br />lent condition after eight years of continuous operation, <br />While the flocculator and clarifier basins were out of service for <br />the winter cleaning and maintenance operations, work on the center <br />well and seal of No, 2 clarifier was completed, The rubber seal was <br />reinforced with a metal band so that it would not suck up into the <br />center well. Extension arms and probing tips were attached to <br />both ends of the scraper. Similar alterations in No. 1 clarifier, <br />completed during the preceding fiscal year, indicated the necessity <br />of this change. <br />Intermittent use of alum as a coagulant had resulted in the accu- <br />mulation of a gelatinous precipitate of aluminum hydroxide in the <br />gravel underbed of the zeolite softeners. The effect of this material <br />was to cement the gravel with the result that the incoming water <br />and regenerating brine channeled through the softener units, The <br />cemented gravel underbeds were removed and new gravel was in- <br />stalled in all the units. When the zeolite was replaced, the defi- <br />ciency in volume of some units was made up with newly purchased <br />siliceous zeolite, Unit No, 12 was held empty until the shipment <br />of high-capacity resinous exchange material was received. This <br />was the first unit in the plant to utilize an exchange material other <br />than synthetic siliceous zeolite. The operation of this resinous ex- <br />changer from the time of installation until the end of the fiscal <br />year confirmed all the promising reRults obtained in earlier pilot <br />plant tests. <br />The use of chlorine-activated silica instead of alum as an aid to <br />coagulation during the lime softening step in plant operation was <br />started, and the results proved very satisfactory. Filter runs were <br />improved and savings in chemical costs were effected through this <br />change. <br />