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1993-04-27_REVISION - M1977378 (2)
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1993-04-27_REVISION - M1977378 (2)
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Entry Properties
Last modified
1/27/2021 8:06:48 AM
Creation date
6/15/2012 6:41:40 AM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1977378
IBM Index Class Name
REVISION
Doc Date
4/27/1993
Doc Name
Response
From
John F. Abel, Jr.
To
Sunnyside Gold Corp
Type & Sequence
TR14
Media Type
D
Archive
No
Tags
DRMS Re-OCR
Description:
Signifies Re-OCR Process Performed
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L:•R. Perino Page 10 Dril 27, 1993 <br /> coarse aggregate concrete bulkheads initially bypassed brine <br /> through multiple pipes, flowing at a rate that increased from 700 <br /> to 6000 gpm under a constant 250 psi of hydraulic back pressure. <br /> Neither bulkhead was notched into the ribs, despite the fact the <br /> cross section of the boring machine cut entry was smooth and <br /> planar, the salt compression strength was probably less than the <br /> concrete strength and neither bulkhead was grouted. The 6-foot <br /> thick bulkhead was constructed over a period of nine days and <br /> failed by leakage and solutioning of the salt around one side, but <br /> not by thrust. The final, successful, 50-foot thick bulkhead, was <br /> built in three parts, a first 10-foot thickness, a second 15-foot <br /> thickness and a final 25-foot thickness over a total period of <br /> twelve days. Twelve days later the 50-foot thick bulkhead was <br /> converted to a permanent bulkhead, able to withstand the potential <br /> 3000 feet of head (1300 psi) by extending its length 37 feet with <br /> unreinforced concrete to a total of 87 feet, notching that section <br /> into the ribs, pressure grouting the salt-concrete contact for the <br /> 37-foot long section through 110 two-inch diameter grout pipes and <br /> bulk grouting over 11040 tons of cement to fill the entire room <br /> behind the 87-foot long bulkhead. The continued operation of the <br /> Rocanville Mine necessitated protection from any possible leakage <br /> and solutioning of the soluble salt. <br /> Scaling of the Sunnyside Mine bulkhead locations will remove <br /> any loose pieces of latite present on the roof, walls and floor. <br /> In addition, the uniaxial compression strength testing samples <br /> included apparently weaker natural joints coated and cemented with <br /> a white mineral. Blast induced fractures in the rock immediately <br /> adjacent to the tunnel will probably permit loosened rock to be <br /> barred out of the tunnel walls but will not produce a smooth <br /> sliding surface for bulkhead movement parallel to the tunnel axis. <br /> Figure 1 presents the blast damage zones adjacent to a <br /> fully-coupled blasthole in massive rock (Morhard et al, 1987, p <br /> 175) . At the Sunnyside Mine the exposed ribsides appear to be in <br /> the least fractured zone, Zone 4 on Figure 1. The perimeter <br /> blastholes in each tunnel round are, of necessity angled outward <br /> in the direction of advance in order to maintain the required <br /> clearance envelope and to permit the holes to be drilled. The <br /> result is an irregular saw-toothed tunnel wall profile which <br /> increases the wall irregularity. <br /> Blast fractures are radial to the individual blastholes and <br /> are limited in extent. Calder (1977, p 6) reported the radius of <br /> rupture around blastholes in various rocks using different <br /> explosives. He reported that the blast damage zone (radius of <br /> rupture) around fully-coupled, ANFO loaded, 2-in. diameter <br /> blastholes in Lithonia granite extended a maximum distance of <br /> approximately 2 feet, 12 diameters, from the center of the hole. <br /> Morhard, et al (1987, p 177) presented a compilation of blast <br /> damage zones. For hard rock, such as the latite at the Sunnyside <br /> Mine, the rupture radius ranged from 7 to 15 diameters of the <br /> blasthole from the center of the blasthole. Blasting probably <br /> produces a zone of increased permeability adjacent to the tunnel <br /> but not a path for bulkhead failure under thrust. <br />
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