Laserfiche WebLink
After the repair, 26 new surface monitor points (2001 through 2026) <br /> were established to monitor the effectiveness of the repair. Through <br /> December 1996, all 26 post-repair monitor points remained stable <br /> with maximum displacements of less than 0.1 ft. Based on these data, <br /> the existing'reconfigured benches and toe buttress appear stable. <br /> 7. Results <br /> ' Haley & Aldrich analyzed the failure through geometric analyses of <br /> the subsurface data and by performing numerical slope stability <br /> analyses using XSTABL. Numerous repair options consistent with <br /> t the existing permit constraints were considered and the preferred <br /> "fix" was to 1) construct a temporary, unreinforced buttress to <br /> immediately support the toe of the slide, 2) unload the top of the slide <br /> ' mass via excavation, and 3) replace the temporary buttress with a <br /> narrower reinforced earth buttress that could only be constructed <br /> safely after unloading at the top was complete. Key to the repair <br /> ' strategy was the geometry of the slide feature which was at a shallow <br /> angle near the toe and steeper near the head. The plan and profile <br /> sheets included in Appendix E labeled "Stage I" through "Stage III" <br /> ' illustrate these three repair steps as originally proposed. A <br /> hypothetical, simplified, slide plane geometry assumed based on the <br /> above-described data for the purpose of affecting a repair design is <br /> shown on the sketches. <br /> It was decided to perform some additional excavation and probe hole <br /> ' drilling on the fourth bench to better define the topography of the <br /> older, underlying, rock bench to see if it might be possible to leave <br /> the temporary buttress as the permanent buttress without <br /> reinforcement. In so doing, it was discovered that the older <br /> underlying bench was partly missing further east (into the hillside) <br /> than previously believed in front of the slide area and buttress limiting <br /> available room to leave the temporary buttress as permanent. <br /> ' Again, viable options were reassessed, but this time including options <br /> that allowed more room to maneuver by moving the mining limits to <br /> ' the east at the top of the hill. The solution that was agreed upon was <br /> to remove the temporary unreinforced buttress and then replace it <br /> later, move the mining limits east to the Limits of Disturbance within <br /> ' the existing permit to gain additional room to work via a Technical <br /> Revision, and adjust the orientation of the highwalls more <br /> southeasterly south from the slide area. The temporary condition of <br /> no buttress had a lower factor of safety (FS = 1.2 to 1.3) than exists <br /> with the permanent buttress, but was acceptable for a short term <br /> situation given the nature of the facility. The key was having some <br /> ' additional room at the top from which to further flatten the slope, if <br /> necessary, if additional movement occurred after the temporary <br /> ' 14 G:\PROJECTS\20200\002\96ANNRPT.WPD <br /> •® w <br />