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TR /ENVIRONMENTAL, INC. <br />A Texas Research International Company <br />• <br />Hydraulic Conductivity <br />Client: Venture Resources TRI Log#: E2337-21-10 <br />Project: Hukill Gultch Millsite Test Method: ASTM D 5084, Method C <br />Sample: Slimes Fraction Test Date: 04/22/10 <br />• <br />• <br />1. E-03 <br />E <br />1. E-04 <br />.y <br />u <br />7 <br />1.E-05 <br />U <br />Hydraulic Conductivity vs. Pore Volumes <br /> _7 7- <br /> <br /> <br /> <br /> <br />- _ <br />_ -= - -_ _ __- <br />_ <br />0.00 0.02 <br />1E06 <br />0.04 0.06 0.08 0.10 <br />Pore Volume (cc) <br />Hydraulic Conductivity vs. Time <br />LE-03 <br /> <br /> t . <br />_ ?' - - <br /> <br /> <br />? _ <br />- - -- - ; - <br /> <br />T <br />rJ4zL <br />f r-T ? i ? d <br />+ ?-- <br />1. E-0 <br />0.0 0.5 1.0 1.5 2.0 2.5 3.0 <br />Time (hours) <br />Q <br />E <br />LE-04 <br />0 <br />b <br />1. E-05 <br />x? <br />6 <br />INITIAL VALUE S <br />Sample Height (in) 1.50 <br />Sample Diameter (in) 2.80 <br />Wet Weight (g) 271.6 <br />Sam le Area 6n2 6.16 <br />Sample Volwne (cc) 150.9 <br />Moisture content (%) 19.92 <br />Wet Density (pcf) 112.3 <br />Dry Density (pcf) 93.7 <br />G, (asswned) 2.65 <br />Degree of Saturation 68.9 <br />Void Ratio 0.77 <br />Porosity 0.43 <br />1 Pore Volume (cc) 65.5 <br />Eff. Confining Stress (psi) 69.4 <br /> Hydraulic Conductivity <br />Time (hrs) k (em/sec) k at 20 deg C <br />(cm/sec) <br />0.20 4.6E-06 4.5E-06 <br />0.33 4.6E-06 4.5E-06 <br />0.62 4.0E-06 3.9E-06 <br />0.80 3.9E-06 3.8E-06 <br />1.02 3.4E-06 3.4E-06 <br />1.28 3.6E-06 3.5E-06 <br />2.12 3.8E-06 3.7E-06 <br />2.35 3.7E-06 3.6E-06 <br />2.53 3.8E-06 3.7E-06 <br />Ava. fe 20 = • 3.51-06 <br />Note 1: The soil was air dried and passed through a No. 100 sieve. Soil 1: Average corrected hydraulic conductivity <br />was remolded a target dry density of 85 % standard Proctor at +4% wet (11-20) is obtained from the last 4 average <br />optimum moisture content or 92.7 lb/ft3 dry density at a moisture content readings. <br />of 20.1 %. Specimens was prepared using Harvard compaction tamper of <br />0.5-in lifts with Imeading compaction. <br />, 04/26/10 <br />Note 2: A I3-value of 0.96 was achieved. The effective confining pressure ChAnalysiseng-Wei <br />Quality Chen, 04126//0 <br />was 69.4 psi (, 10;000 psf) per test request. <br />Tested by: Caleb McCord <br />The testing herein is based upon accepted industry practice as well as the test method listed. "rest results reported herein do not apply <br />to samples other than those tested. TRI neither accepts responsibility for nor makes claim as to the final use and purpose ofthe material. <br />TRI observes and maintains client confidentiality. TRI limits reproduction ofthis report, except in full, without prior approval of TRI. <br />9063 Bee Caves Road ? Austin, TX 78733-6201 ? (512) 263-2101 ? (512) 263-2558 ? 1-800-880-TEST