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2009-07-15_REVISION - M1980244 (23)
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2009-07-15_REVISION - M1980244 (23)
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Last modified
6/15/2021 5:52:22 PM
Creation date
7/21/2009 11:01:54 AM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1980244
IBM Index Class Name
REVISION
Doc Date
7/15/2009
Doc Name
QA Mon. & Test Results Load Out- Bin Location
From
CC&V
To
DRMS
Type & Sequence
AM9
Media Type
D
Archive
No
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• <br />C] <br />L1 <br />Cripple Creek & Victor Gold Mining Company <br />Cresson Project <br />Quality Assurance Monitoring and Test Results <br />Load Out Bin Relocation <br />July 7, 2009 <br />¦ Caterpillar 330 Trackhoe (2); <br />¦ Caterpillar 375 Trackhoe; <br />¦ Caterpillar 385 Trackhoe; <br />¦ John Deere 850 Rubber Tire Backhoe; <br />¦ Komatsu 800 Trackhoe; <br />¦ Volvo A40D Haul Trucks (8); <br />¦ T360 Forklift <br />¦ Caterpillar 777 Haul Trucks (6); and <br />¦ Tamrock 700 and 1100 Drill Rigs (6 total). <br />amecs <br />Table 2 presents a summary of the weather during the period of April 3rd through May 6th, 2009 <br />for the LOB relocation construction activities. <br />2.1 Underground Workings Remediation <br />Historic underground workings within the footprint of the LOB were remediated following the <br />recommended remediation plans presented on Drawing No. A290 of the IFC Drawings. <br />The majority of underground workings (listed on Table 3) were removed during site grading <br />activities. Only one working required remediation. This working (No. 2019 located at N 54641.4 <br />and E 37585.9) consisted of a shallow shaft (approximatel 25 feet) with two small adits. <br />Exploratory drilling was conducted around the shaft to a minimum depth of 50 feet. The results <br />of the drilling determined that the adits did not extend beyond 5 feet from the shaft edge. This <br />working was remediated by removing the crown pillars of the adits and loose rock with a track <br />excavator. Once the loose rock was removed, the working was inspected by the Certifying <br />Engineer and then backfilled following the shallow shaft remediation presented on Drawing No. <br />A290. <br />All exploratory drillholes that did not intercept underground workings were completely grouted <br />with bentonite slurry prior to remediating the working. <br />2.2 Site Grading <br />Prior to SF placement, Ames conditioned and compacted the subgrade surface of the fill area. <br />AMEC monitored the preparation of the subgrade and verified that it met project specifications. <br />SAPROJECTS11125E CCV CQA\H3 - CONSTRUCTIOMLOB CERT REPORT\REPORT BOD`I\LOB CERT REPORT 2009.07.07.DOC <br />6
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