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:: <br />. J. E. STOVER & ASSOCIATES <br />' 2768 COMPASS DRIVE, SUITE 101 <br />GRAND JUNCTION, COLORADO 81506 <br />PHONE: (303) 245-4101, FAR 242-7908 <br />MINE ENGINEERING <br />MINE RECLIUMTION <br />July 10, 1995 <br />A. J. Waldron <br />Division of Minerals and Geology <br />1313 Sherman St., Room 215 <br />Denver, CO 80203 <br />Re: Somerset Mining Company <br />East Yard Pond - TR-026 <br />Permit No. C-81-022 <br />Dear Mr. Waldron: <br />III IIIIIIIIIIIIIiII <br />sss <br />CIVIL ENGINEERING <br />CONSTRUCTION MANAG <br />~'~~EIVED <br />JUL 121995 <br />Division o~ ~~~i~~erals & Geology - <br />The Division's letter dated June 14, 1995 transmitted its adequacy <br />review for the referenced technical revision. The intent of the <br />technical revision was to address a concern you expressed during a <br />recent field inspection regarding the spillway configuration of the <br />east yard pond. Specifically, you noted the crest elevation of the <br />primary and emergency spillways were not separated by the required <br />one foot as required by Rule 4.05.6(4). The Division developed <br />additional questions and concerns about the design of the east yard <br />pond during its review of the technical revision. Following are <br />Somerset's responses to the Division's concerns: <br />1. The run-off volume from the 25-year event is presented on page <br />B-38. The 25-year 24-hour event produces 10,236.67 cubic feet <br />of run-off volume. The soil loss calculation presented on <br />page B-39 produces a 3 year sediment storage volume of 2000.28 <br />cubic feet. The maximum sediment and water level from the 25- <br />year event is presented on the staging chart on drawing ES- <br />3404. The revised drawing C8-1166 submitted with the original <br />technical revision application should be disregarded since <br />this information is now presented on revised map EB-3404. <br />2. The run-off volume from the 10-year event is presented on page <br />B-38. The 10-year 24-hour event produces 6,349.96 cubic feet <br />of run-off volume. Since the pond will contain the run-off <br />from the 25-year event, the water level generated from the 10- <br />year event was not shown on drawing E8-3404. The information <br />presented on new page B-39a shows that the emergency spillway <br />should be upgraded to a 12" CMP. <br />Somerset does not believe the entire hydrologic design of the <br />east yard pond needs to be amended. The hydrologic design <br />presented on pages B-35 through B-39 has been a part of the <br />approved permit document for 14 years. The east yard pond has <br />