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ENFORCE27394
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ENFORCE27394
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Entry Properties
Last modified
8/24/2016 7:35:02 PM
Creation date
11/21/2007 11:36:22 AM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1978052
IBM Index Class Name
Enforcement
Doc Date
12/4/2001
Doc Name
FAX TRANSMITTAL
From
LIDSTONE & ASSOCIATES INC
To
DMG
Media Type
D
Archive
No
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Dec-Q4-01 O2:24P • • P_O5 <br />Mr. Jell' Schwari <br />Uecem6cr 4, 2nn 1 <br />Page 4 <br />O.OOlS fVft, which was slightly greater than the measured bed slope (5.001 ft/ft: established using the <br />Epp and Associates survey data). LA's divergence from tneasurcd bctl slope is justified in that the water <br />surface energy slope rather than the channel slope is an essential element in this calculation. Under lower <br />flood tlow conditions, the effect of the Branhter will also eel lv steepen the energy ,lope. The decision to <br />use a slope of 0.0015 is further validated by tield evidence that supports cltanncl's cunlaittment of events <br />Lower titan 6000 cfs. Al a slope of 0.001, tltc river wvt+ld overtop the bank at 5000 cfs, rather titan 6500 <br />cfs. Historic evidence doesn't support this. <br />Assuming there are no pre-existing "breaches" in the cltattttcl bank, stage discharge curves were <br />developed at the nvrlhem and southern "breach cross section location" (Tahlcs 1 and 2). The ttorntal <br />depth analysis fur the northern breach indicates that the levee begins to overtop al 6,SOU cfs (Reference <br />Table 1 where a stage Iteigltt of 10 feel is cyual tv 5038.6 feet). Normal depth analysis of the svuthcm <br />breach indicates that the Ievice will nut be overtopped wail the dischsrge is in excess of 8,000 cfs (please <br />reti:rettce Table 2 where a stage height of 9 fi:et equates l0 5038 feet). In January 2001, a photo was taken <br />by Llrban Drainage (Figure 3.1) which indicates the presence of art erosion cut (i.e., the area ot'tlte May 5, <br />2001 breach) at the north Ivcalivn. LA has estimated that this "cut" was approxima[ely four (4) feet deep <br />and 10 feet wide (see attached photo). Assuming the top of bank is elevation of 5039, the invert of the <br />cut is 5035. This would suggest that flow would begin to enter tltc "cut" and discharge from the South <br />Platte River to the Bull Seep Slvugh, when the main channel is flowing around 2600 ct's. <br />Tables 3 and 3A present hydraulic analyses of the assumed dimensions initial breach using the weir <br />equaticn CI,H`n. Depending on the assumed sii4 of the erosion cut (4 versus 6 feel deep), somewhere <br />from 266 cfs to 490 cfs stay have passc<I through the "erosion eul" at the northern breach location <br />assuming that the geometry of the "erosion cut" remained unchanged during the May 5, 2001 event. This <br />is an unlikely scenario and LA concludes that as mute and more Clow passed through the May 5, 2001 <br />breach, the erosivtt cut progressively enlarged wail failure was achieved. Because the levee was <br />constructed of nun-engineered fill material, once water started tlowittg through the breach, failure <br />occurred quite rapidly. Llltimatcly the breach enlarged to an opening apprvxitnately six (6) to seven (7) <br />feet deep by 100 feet Inng based on Geld observations of the breach repair which occurred at the Cnd of <br />Mey, 2001. Table 4 presents a rating table fvr tltc hrcach utilizing these enlarged dimensions. <br />Normal depth analyses were perfbrnted for the Bull Seep Drain et cross sections approximately 200 fact <br />upstream and 800 tear downstream oC the north breach (Table 5 grid 6 rnspectively)• To complete the <br />normal depth analysis, a roughness coefficient of 0.035 and an average slope of 0.003 fl/fl was assumed. <br />Table 5 identifies the actual pre-flood capacity (400 cfs) of the Bull Secp drain, Yertnit M-78-052 <br />(M!'M's reclamation permit) required s capacity of 350 cf's. Table 6 reflects the conveyance capacity of <br />the pre-flood Aull Seep Slvugh below the Nortlt Breach. Neither the existing trot the pcmtittcd Hull Seep <br />T.)rsin ('!'able S), upsttrrutt of the Bull Seep Slough could convey the flood even! of May 5, 2001 (>I500 <br />cfs: Table 6). Witlt this said, the locstivn of the Hu11 Seep Drain wuultl not make arty difference with <br />respect to dowttstreartt material damage within the Bull Seep Slough. <br />It is 1.A's uttderstattdi+tg that a hrcach did exist at the southern location at the time of the May 5, 2001 <br />event. The dimensions of this breach at the time of the May flood evert are unknown but field evidence <br />indicates that; (I) the ittveR of this breach was higher tlton the nnrlhem breach; (2) the conveyanec <br />capacity of the river cross section at this location was greater than its downstream counterpart; and (3) <br />due to the geometrical configuration of this hresch (off-channel from the South Ylatte) that development <br />of the opening would be limited. The potential impact of the southern breach an the Bull Seep Slough as <br />
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