My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
HYDRO26395
DRMS
>
Back File Migration
>
Hydrology
>
HYDRO26395
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
8/24/2016 8:45:55 PM
Creation date
11/20/2007 6:36:35 PM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1999002
IBM Index Class Name
Hydrology
Doc Date
9/20/2004
Doc Name
P&A Reports
From
American Soda L.L.P.
To
DMG
Media Type
D
Archive
No
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
22
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
Fonn 31605 UNITED STATES Eoast ArrEOVEo <br />Qune 1990) DEPARTMENT OF THE INTERIOR atraget ouneau No. lea-or3s <br /> Ex Tres: hfarch 31, 1993 <br />BUREAU OF LAND MANAGEMENT 5. t e+~e ixslgrmuo~ and serlat No. <br /> Yankee Gulch CO-118328 <br />SUNDRY NOTICES AND REPORTS ON WELIS <br />Uo not use this form for proposals to drill or ~ deepen or reentry to a different reservoir. s. uma;mr, eWOthe or tribe Name <br />Use "APPLICATION FOR PERMfC--" for such ro N/A <br />SUBMITINTRIPI.ICATE 7. uurdt or Gt, A~ax~ent Drsigrution <br /> A <br />f. Type of WeB 8. Well Name and No. <br />^ Oil Well ^ Gas Well ©Other Nahcolite Solution American Soda LLP 7fF76 <br />2. Nwle of Operator 9. API WeE No. <br />American Soda, L.L.P. <br />3. Address and Telephone No. lo. riela and root o. Exgoratory Area <br />2717 C . Rd. 215 Parachute, CO 81635 9711 285-6500 Central Piceance Creek Basin <br />4. Location of Well (Footage, Sec., T., R, M., or Survey Description) u. counry or rarish slave <br />E 12622.79 N 13007.% SW r/a of SE r/s of Section Z0, TIS, R97W 6m P.M. Rio Blanco, CO <br />TYPE OF SUBMISS[ON ~ TYPE OF ACTION <br />^ Notice of Intent <br />l7Subsequent Reports <br />OFinal Abandonment Notice <br />© Abandonment <br />^ Recompletion <br />^ Plugging Back <br />^ Casing Repair <br />^ Altering ('acing <br />Other. <br />O Change of Plans <br />^ New Construction <br />^ Non-Routine Fracturing <br />^ Water Shut-0ff <br />~ Conversion to Injection <br />^ Dispose Water <br />(Nqr. FePus msolmNmvitipkmmris,onm Well <br />17. Rao~IDe Propmedm COmPkmd Ope++tiom(~+rly sere all patvn~tdtteils,aM A~TPeM~eem data. indudiry{esminted dam of uartmg anY CroMeN wmt It we~bdmatimWlY drWed. pJ~c suNUAam lantiom <br />.md mmured and true •ertirul degln (maa ma4ers and m~ peament m duv wmkr <br />We1120-76 dissolution surface at 1624'. <br />6/11/2004 Rig up Key Fatergy on well and pull all (2427) of 4 tfe" long string . <br />6/12/200.1 Pull all (7244') of 4 rfz" short string. Set cast iron bridge plug in long T' casing string at 190(1' <br />6/]4/2003 Set castiron bridge in short T' casing string at 1900'. <br />An MIT was performed on 8/26/04. The long T' casing string failed the MIT. <br />On 9/6/04, Cudd Pressure Control tripped coIl tubing to the bridge plugs and 1-Ialliburton pumped 263 sacks of Type G, 35% SSA-1, 0.2% <br />CFR„', 15.6 #/gal, 1.55 ft3/sack cement in each T' rasing string for a total of 526 sacks (or Me welt <br />The wellhead E scheduled for cutdown on 9/14/04 <br />14. f hereby certify that the foregoing is true and cortect. <br />Signed <br />(This spare for Federal or State office use) <br />Approved by Tide Date <br />Conditions of approval, B any: <br />TiOe 1S U.S.C. Section 1001, makes it a crime for any person knowingly and willfully to make to any department or agency of the Unified <br />States any false, fictitious or fraudulent stateme<lts or representations as to any matter within its jurisdiction <br />'See Instnrction on Reverse Side <br />
The URL can be used to link to this page
Your browser does not support the video tag.