Laserfiche WebLink
Sane/ <br />rte.- i.unia■�a►w •i•���- =.a��.anr.��.�.� <br />Sle!! FKV" ") li w Vvi <br />Pumping <br />Service Report <br />9144399 <br />Treatment Report <br />Event # Event Time Event Description <br />Fluid Type <br />Rate <br />Tubular Pressure <br />Annular Pressure <br />Stage Volume <br />Total Volume <br />bbl /min <br />si <br />si <br />(bbl) <br />(bbl) <br />1 Sep 11,2014 06:00 Arrive On Location <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />0.00 <br />2 Sep 11,2014 06:10 Tailgate Meeting <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />0.00 <br />3 Sep 11,2014 06:20 Safety Meeting <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />0.00 <br />4 Sep 11,2014 06:30 Sign -off on Safety <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />0.00 <br />5 Sep 11,2014 07:00 Rig In <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />0.00 <br />6 Sep 11,201411:22 Pressure Test <br />Water <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />0.00 <br />Remarks: Test Sanjel Lines <br />7 Sep 11,201411:38 Pressure Test <br />Water <br />0.00 <br />370A <br />0.0 <br />0.00 <br />0.00 <br />Remarks: Test Casing <br />8 Sep 11,2014 12:20 Wait On Instructions <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />0.00 <br />Remarks: Wait on perfing operations <br />9 Sep 11,201414:46 Pressure Test <br />Water <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />0.00 <br />Remarks: Test Sanjel Lines <br />10 Sep 11,201414:47 Pump <br />Water <br />2.50 <br />2,000.0 <br />0.0 <br />10.00 <br />10.00 <br />Remarks: Establish Circulation <br />11 Sep 11,201414:53 Pump <br />0:1:0 Type <br />III <br />2.50 <br />2,800.0 <br />0.0 <br />23.60 <br />33.60 <br />12 Sep 11,201416:03 Pump <br />Water <br />2.50 <br />1,800.0 <br />0.0 <br />8.50 <br />42.10 <br />-- Remarks: Displace cement out of coil and to 1621' <br />Sep 11,201416:10 JSA <br />- <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />42.10 <br />Remarks: Pre rig out meeting <br />14 Sep 11,201417:00 Rig Out <br />- <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />42.10 <br />15 Sep 11,2014 17:55 Pre - Departure Meeting <br />- <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />42.10 <br />16 Sep 11,201418:00 Job Complete <br />- <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />42.10 <br />17 Sep 11,201418:00 Leave Location <br />- <br />0.00 <br />0.0 <br />0.0 <br />0.00 <br />42.10 <br />Did Float Hold: Not Applicable <br />Fluid Returns : Not Expected <br />Type : <br />Volume (bbl) : <br />Temperature ( °F) <br />FDAS Functioning Correctly: Yes <br />Was the Program Followed As Per Design?: Yes <br />Material Transfer Sheet Number <br />Material Transfer Sheet Number <br />6998 <br />Comments To Service Report <br />Job went good and was pumped as per customer request. During the 30 minute pressure test the well showed a loss of 6 PSI total. Once the well was full it <br />took about 10 gallons to pressure up to 370 PSI_ After the thirty minutes the same amount of water was recovered when the pressure was blead off. <br />Acidizing • Cementing • Coiled Tubing • Fracturing • Nitrogen <br />Canada • USA • International <br />Print Date: September 11, 2014 <br />Service Report: 9144399 <br />Page 3 of 3 V3.12.0.0 <br />