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2014-11-04_HYDROLOGY - M1988112
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2014-11-04_HYDROLOGY - M1988112
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Last modified
8/24/2016 5:55:13 PM
Creation date
11/5/2014 8:49:01 AM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1988112
IBM Index Class Name
HYDROLOGY
Doc Date
11/4/2014
Doc Name
San Luis Project Tailing Dam Annual and 3rd Quarter Reports.
From
Battle Mountain Resources, Inc.
To
DRMS
Permit Index Doc Type
Hydrology Report
Email Name
WHE
Media Type
D
Archive
No
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DAM NAME: San Luis Tailing Dam <br />DATE OF REPORT: 05/15/14 <br />Condition does not currently threaten impoundment but needs repair and possible riprap to prevent future <br />erosion. <br />TAILING DAM INSPECTION FORM <br />Directions: Mark and X for conditions found and underline words that apply <br />SEEPAGE AND DRAIN OUTFALL <br />PROBLEMS NOTED: ❑ (30) NONE <br />❑ (31) SATURATED EMBANKMENT AREA ❑ (32) SEEPAGE EXITS ON DAM <br />❑ (33) SEEPAGE EXITS AT POINT SOURCE <br />0 (34) SEEPAGE AREA AT TOE <br />DRAIN OUTFALL SEEN: ❑ YES 0 NO <br />0 (35) FLOW ADJACENT TO DRAIN PIPE ❑ (36) DRAIN OUTFLOW TURBID <br />0 (38) OTHER: Three subdrain lines for tailings impoundment. All are covered due to local <br />❑ (37) DRAIN DRY /OBSTRUCTED <br />slumping. Drains need to be uncovered. <br />SHOW LOCATION OF DRAIN ON SKETCH <br />AND INDICATE AMOUNT AND QUALITY OF SEEPAGE <br />See 2013 Detailed Inspection Report for location; approximately 30 gpm clear flow <br />CONDITIONS OBSERVED: <br />❑ GOOD ❑ ACCEPTABLE ❑ POOR <br />STORM WATER MANAGEMENT SYSTEM <br />PROBLEMS NOTED: ❑ (40) NONE <br />❑ (41) NO EMERGENCY SPILLWAY <br />❑ (42) EROSION AT DROP STRUCTURE <br />❑ (43) CONCRETE DETERIORATED /UNDERMINED ❑ (45) STRUCTURE MAY BE TOO SMALL <br />❑ (46) DIVERSION CHANNEL EROSION <br />❑ (47) INADEQUATE CHANNEL FLOW CAPACITY ❑ (48) CHANNEL FLOW OBSTRUCTED <br />D (49) OTHER: See 2013 Detailed Inspection Report for hydraulic analyses regarding Drop Structure <br />CONDITIONS OBSERVED: <br />❑ GOOD 0 ACCEPTABLE ❑ POOR <br />MONITORING <br />EXISTING INSTRUMENTATION FOUND: <br />❑ (50) NONE ❑ (51) GAGE ROD IN POOL AREA 0 (52) PIEZOMETERS <br />❑ (53) SEEPAGE WEIRS /FLUMES <br />❑ (54) SURVEY MONUMENTS ❑ (55) OTHER <br />MONITORING OF INSTRUMENTATION: <br />❑ (56) NO 0 (57) YES <br />PERIODIC INSPECTIONS BY: <br />0 (58) OWNER ❑ (59) ENGINEER <br />See attached piezometer measurements <br />CONDITIONS OBSERVED: <br />0 GOOD ❑ ACCEPTABLE ❑ POOR <br />MAINTENANCE AND REPAIRS <br />PROBLEMS NOTED: ❑ (60) NONE <br />❑ (61) ACCESS ROAD NEEDS MAINTENANCE ❑ (62) CATTLE DAMAGE <br />❑ (63) BRUSH ON: UPSTREAM SLOPE /BEACH, CREST, DOWNSTREAM SLOPE, TOE <br />❑ (64) RODENT ACTIVITY ON: UPSTREAM SLOPE /BEACH, CREST, DOWNSTREAM SLOPE, TOE <br />0 (65) OTHER: erosion gully repairs needed <br />CONDITIONS OBSERVED: <br />0 GOOD ❑ ACCEPTABLE ❑ POOR <br />Page 2 of 4 <br />
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