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2014-08-19_REPORT - M1980244
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2014-08-19_REPORT - M1980244
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Last modified
9/6/2020 4:18:09 PM
Creation date
8/20/2014 7:31:20 AM
Metadata
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Template:
DRMS Permit Index
Permit No
M1980244
IBM Index Class Name
REPORT
Doc Date
8/19/2014
Doc Name
Weekly CQA Report: Week ending 08/09/14.
From
CC&V
To
DRMS
Email Name
TC1
Media Type
D
Archive
No
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ameO <br /> Confirmatory drilling was completed at working UG#6551. Additional remediation is required. <br /> Previously drilled confirmatory boreholes were grouted at the Anaconda Mine Complex. <br /> Additional remediation is required. <br /> Working#6543, found to be a shaft, was excavated to approximately 30 feet. The shaft was <br /> backfilled for confirmatory drilling access and drilled. The confirmatory borings were grouted. <br /> Additional remediation is required. <br /> Underground workings, UG#U6532, UG#U6533, UG#U6534, UG#6541, and UG#6580 were <br /> excavated to competent rock, backfilled per project specifications, and are considered <br /> remediated. <br /> Ames started excavating underground working UG#6588. Further remediation is required. <br /> Workings UG#6581 and#6582 were excavated to equipment refusal into hard rock. Drilling <br /> access will be provided and additional remediation is required. <br /> C) Geomembrane: <br /> PSSA <br /> Geomembrane installation continued within the PSSA and included: deployment, seaming, repair, <br /> and QA/QC activities. Approximately 42,086 square feet of 100-mil LLDPE SSMS (secondary) <br /> geomembrane liner was deployed (panels S-248 through S-263). Subgrade was inspected and <br /> approved by AMEC, Ames, and ECA representatives prior to geomembrane deployment. <br /> Approximately 2,089 linear feet of seam was fusion welded during deployment using two fusion <br /> welding machines. Destructive and non-destructive testing was completed per project technical <br /> specifications (Destructs 106 through 107). <br /> Due to weather conditions throughout the week, no additional liner was approved for low volume <br /> placement. <br /> Anchor trench was excavated to approximately station A17+00 on the east side of the PSSA and <br /> to station B12+00 on the west. Anchor trench backfilling occurred immediately after liner <br /> deployment and non-destructive testing was completed. <br /> Large rocks were removed from the anchor trench on the PSSA embankment along the 9,450' <br /> elevation trench using a mini excavator and/or a Cat excavator with a hammer attachment. <br /> D) Overliner: <br /> PSSA <br /> Low volume material was placed up the slope near the LVSCS riser trench for subsequent 18- <br /> inch HDPE pipe installation. Three 400-feet long, 18-inch HDPE pipe sections were placed in the <br /> LVSCS riser trench. <br /> Cat 740 trucks hauled low volume solution collection fill (LVSCF)to the PSSA. Haul roads for the <br /> trucks were maintained at least 4 feet above secondary geomembrane. <br /> Ames continued placing low volume solution collection fill (LVSCF)on approved secondary liner <br /> in minimum 3-foot lifts with Cat GPS D6 and D8 wide pad dozers between panels S80 to S85; <br /> S90 to S102; S118 to S129; S133 to S141; S146 to S148; S187; S207 to S208; and S211 to <br /> S214. <br /> See the attached LVSCF map for all placement locations. <br /> 2014 08 09-MLE2 WEEKLY FINAL.DOCX Page 3 of 7 <br />
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