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("C' <br />kK, <br />ameo <br />Cat dozers graded the slopes downwards near station 06 +00 to Q12 +00 and stockpile shot rock near station <br />A6 +00. <br />A Cat 330 excavator was grading the Y2 to 1 slope on the northwest side of the PSSA area near stations A0 +00. <br />Clay (SLF) Processing: <br />Cameron Site: No Clay mining or processing occurred at the Cameron Site. Approximately, 244,860 tons of clay / <br />soil liner fill (SLF) material have been produced at the Cameron site. SLF produced from the operation remains <br />stockpiled at Cameron Site for later removal / use. <br />Squaw Gulch Clay Borrow Site: Clay processing took place at the Squaw Gulch Clay Borrow Site. <br />Approximately, 19,300 tons of soil liner fill material has been produced at the Squaw Gulch Clay Borrow Site to <br />date. <br />A John Deere 870 excavator was used to load Cat 777 haul trucks with clay till at the upper portions of the Squaw <br />Gulch Clay Borrow area. The till was transported to lower portion of the borrow area for processing. <br />Underdrain System: <br />Secondary Underdrain: Approximately, 200 feet of secondary underdrain was installed between stations C6 +00 <br />and E11 +00 and 810 feet was installed in the Phase 2 diversion Channel area adjacent to Dump. Approximately, a <br />total of 5,064 feet of Secondary underdrain has been completed. <br />Primary Underdrain: No work was performed on the Primary underdrain during this reporting period. A total of <br />1,294.60 feet of Primary underdrain has been completed. <br />Tree /Slash Grubbing and Clearing, Chipping: <br />No clearing and grubbing occurred. <br />B) Underground Workings <br />Confirmatory drilling was performed on underground working No. U6397. All borehole locations were established <br />on a 4 -foot center isolating any voids found. Further remediation efforts will be ongoing until remediated. Summary <br />of the remediation efforts will follow when remediation is completed. <br />UG #6123 was blasted and the shot rock was removed from the working. <br />Two depressions were excavated at UG U6387 to competent rock at depths of 16 feet and 22 feet. The <br />depressions were backfilled using excavated material placed in 18 inch to 25 inch lifts that were compacted using <br />the excavator bucket. <br />C) Highway 67 <br />No significant construction activities were observed at the Highway 67 Realignment. <br />South MSE Wall: <br />No significant activities occurred at the South MSE Wall; however, Ames worked on removing tailings and timbers <br />from the Crib Wall. The timbers will be used as the facade at the south MSE wall; the tailings were stockpiled for <br />later removal. <br />II) Storm Water Management <br />Best Management Practices (BMP) is being performed. Erosion control efforts took place during this reporting <br />period following any precipitation. <br />Page 2 of 6 MLE2 WE 12.21.13.doe <br />