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<br />,; <br /> <br />d <br /> <br />" <br />I <br /> <br />f (.... {" 1 <br />a.'~.&... <br /> <br />" ~ <br /> <br />OPEHATIOS ASD MAINTESANCE <br /> <br />37 <br /> <br />zeolite softening was used. with the result that the h"rdne~s of the <br />plant effluent water was higher than the desired value of 125 parts <br />per m i !lion. <br />The shortage of rainfall and the normal increase in water demand <br />due to growth of population were reflected in the maximum monthly <br />averages of quantity of water softened and in the average daily <br />input to the softening plant. A new peak flow through the plant was <br />reached on July 30 and 31, 1947 when 201.7 cubic feet per second. <br />or 130.4 million gallons per day, were softened_ This is 30.4 per cent <br />above the present designed capacity of the plant. The monthly aver- <br />age rate of inflow ranged from a minimum of 48_6 cubic feet per <br />second, or 31.4 million gallons per day. in December 1947, to a maxi- <br />mum of 170.6 cubic feet per second, or 110.3 million gallons per day, <br />in July 1947. The a\"el'age daily flow through the plant for the fiscal <br />year 1947-48 was 101.2 cubic feet per second. or 65.4 million gallons <br />per day, an increase of 18.9 per cent o\"er the corresponding figure <br />for the preceding fiscal year. <br />Because of the increasing age and wear of the equipment. the <br />incidence of mechanical difficulties has become more frequent and <br />the nature generally more serious_ Seating rings were replaced in <br />three. and hook rods in all of the 36-inch filter wash water valves_ <br />All of the hydraulic c)'linders for operation of the filter sluice gates <br />were overhauled_ New gate leaves were installed in four of the soft <br />water effluent valves in the zeolite building. Chain and sprocket <br />drive units were fabricated for the three lime slakers to replace <br />the belt-driven units which had proved inadequate. The high per- <br />centage of unburned cores in the lime delivered to the softening <br />plant required that each slaker be taken out of service and cleaned <br />of grits after every 100 tons of lime slaked in it. The 15-val\"e <br />chlorine manifold was overhnuled. The carbon dioxide boiler was <br />retubed and a new burner designed and installed in order to increase <br />the carbon dioxide output sufficiently to meet the increased load. <br />Sludge disposal presented one of the most recurrent problems of <br />the year_ Due to repeated shutdowns in sludge pumping occasioned <br />by numerous breaks in the 8-inch vitrified clay sludge disposal line, <br />a 300-foot section of the clay pipe was replaced with 8-inch pl-ecast <br />concrete pipe_ A new sludge pump vault was constructed at thc <br />lower sludge basin and two booster pumps were installed therein <br />to facilitate sludge handling_ <br />Two chlorine evaporators were installed in order to increase the <br />chlorinator output sufficiently to meet the demand at the high rate <br />of flow. A third chlorinator was procured and installed to se"ve as <br />