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PROJ00382
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Last modified
10/5/2010 10:57:00 AM
Creation date
10/5/2006 11:52:06 PM
Metadata
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Template:
Loan Projects
Contract/PO #
C153685
Contractor Name
Monument, Town of
Contract Type
Loan
Water District
10
County
El Paso
Bill Number
SB 94-029
Loan Projects - Doc Type
Feasibility Study
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<br />8 <br /> <br />.- <br />BCJ"'Le~ <br /> <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br /> <br />Chapter III . Background Information <br /> <br />Spillway Width: <br /> <br />130 feet <br /> <br />Spillway Capacity: <br /> <br />11 ,400 cfs <br /> <br />Spillway Crest Elevation: <br /> <br />6918.7 feet <br /> <br />Outlet Works: <br /> <br />Twin 16-inch cast iron pipe <br /> <br />Outlet Capacity: <br /> <br />63 cfs <br /> <br />Several dam safety deficiencies have been noted by the SEa, which include the <br />following: <br /> <br />I. Upstream Slope: Poor condition due to the thick tree and brush cover and erosion gullies <br />up to 2-foot in depth. <br /> <br />2. Crest: Poor condition due to large trees along the crest, deep erosion gullies up to 3-foot <br />deep. <br /> <br />3. Downstream Slope: Poor condition due to large trees, brush, and deep erosion gullies. <br /> <br />4. Seepage: Unacceptable condition due to seepage under spillway structures. <br /> <br />5. Outlet Works: Poor condition due to a left gate failure and condition of the existing outlet <br />pipe. <br /> <br />6. Spillway: Poor condition due to inadequate spillway capacity, back cutting erosion at the <br />lower cutoff wall and the failed gabion structure along the right lower end of the spillway. <br /> <br />The SEO has rated the dam to be in "very poor" condition and in immediate need of <br /> <br /> <br />major repair. The reservoir is presently restricted three feet below the spillway crest due to the <br /> <br /> <br />inadequate spillway capacity and the structural condition of the spillway. <br /> <br />A site visit of Monument Lake Dam was performed on February 19,1999. The following <br />features of the dam were reviewed: upstream face of the embankment above the reservoir; dam <br />crest; downstream face of the embankment; left and right abutments of the embankment; <br />downstream toe area of the embankment; spillway and downstream channel; outlet works pipes <br /> <br />Monument Lake Dam Feasibility Study <br />
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