My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
HYDRO25674
DRMS
>
Back File Migration
>
Hydrology
>
HYDRO25674
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
8/24/2016 8:45:20 PM
Creation date
11/20/2007 5:47:37 PM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
C1989074
IBM Index Class Name
Hydrology
Doc Name
RIMROCK MINE SEDIMENT POND CERTIFICATION
Permit Index Doc Type
SEDIMENT POND INSPECTIONS
Media Type
D
Archive
No
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
Page 1 of 1
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
~ ~ III IIIIIIIIIIIIIIII <br />Rimrock Mine Sediment Pond Certification <br />The site inspection was conducted on March 31, 2000 1[ was a partly sunny day of 36 <br />degree temperature and it appeared that no precipitation had occurred in the previous <br />week. The pond was mostly dry except for 3 inches of water in the low area near the <br />principal spillway inlet. There were signs of snowmelt in the past two weeks although <br />the pond showed no sign of discharge. The surface was wet from the snowmelt in the <br />shade and was dry in the sunshine. The pond itself was free of any type of problem <br />with stability or erosion. Engleville Gulch was also dry. The pond is to be left as a <br />permanent impoundment for use in the grazing operation. <br />The following items were checked to see if they coincided with the design shown in <br />the mine permit application. I, Greg Lewicki, did the pond design in March of 1990. <br />1) Constructed Elevations: The elevations listed below were checked with a precision <br />level and stadia rod: <br />-Dewatering pipe inlet <br />-Dewatering pipe outlet <br />-Top of Dam <br />-Bottom of Emergency Spillway <br />-Toe of Dam (outside and inside) <br />-Bottom of Pond <br />-A number of points within the pond <br />All elevations were found to be acceptable. The inlet to the principal spillway was <br />placed at a slightly higher elevation to allow more sediment storage. The 10 year - 24 <br />hour runoff storage was still present above the principal spillway. <br />2) Width of Emergency Spillway Design: 12 feet. Measured: 12.2 feet. <br />3) Depth of Emergency S~Ilway Design: 1.55 feet. Measured: 1.60 feet. The spillway <br />showed no evidence of flow or any signs of erosion or other instability. <br />4) Width of to~of Dam Design: 10 ft. Measured: 10.2 ft - 10.6 feet. <br />5) Principal Spillway Design: 4.0" pipe placed in compacted embankment. Measured: <br />4" steel pipe placed in compacted embankment. Extensions on this pipe were added to <br />both sides so that the embankment could be widened. Some black plastic hose was also <br />present near the spillway at the time of the inspection but was not functional. The <br />principal spillway pipe was completely free of debris and was functional during the site <br />visit. <br />
The URL can be used to link to this page
Your browser does not support the video tag.