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f L. Perino Page 2 uary 31, 1994 <br /> concrete mix was as specified except that the maximum aggregate <br /> size was reduced to 3/8-inch from the original 3/4-inch to <br /> facilitate placement through the slick-line. A pre-measured and <br /> bagged plasticizer ("SupercizerTMI,) was added to each batch of <br /> concrete to further facilitate placement through the slick-line. <br /> The specified 16 percent of fly ash was included in each pre- <br /> mixed and pre-measured bag. Additional cement was added to <br /> maintain the specified strength, which was verified by testing <br /> before the formulation was accepted for purchase and placement. <br /> The remote controlled fill hose permitted complete filling <br /> of the bulkhead to within 1-foot of the back of the tunnel. The <br /> fill pipe used for filling the final foot of the bulkhead <br /> restricted flow of concrete into the bulkhead form. This did not <br /> cause a problem except when the injected concrete engulfed the <br /> fill pipe. It may be possible to use a slightly larger diameter <br /> final fill pipe and larger bulkhead openings at the top of the <br /> form. <br /> The placement of the extremely low slump and low <br /> water/cement ratio concrete was facilitated by the ingenious <br /> remote controlled vibrator set-up. Filling to the back of the <br /> bulkhead would be speeded-up by developing a method of stiffening <br /> the vibrator hose, possibly by tapping the hose to a 1 x 1-inch <br /> angle iron. <br /> It appears that the speed of filling future <br /> bulkheads can be facilitated by inserting a smaller screen over <br /> the concrete pump feed bin to screen out the occasional coarse <br /> lump of pre-set concrete that had somehow formed during transport <br /> and storage of the pre-mixed concrete. The cement content of the <br /> pre-mixed concrete appeared to be more variable than anticipated. <br /> Some of the batches in the concrete mixers were obviously dryer <br /> than others and in those cases the water/cement ratio was <br /> increased to 0.46. The water/cement was increased to 0.49 for a <br /> very limited number of batches to permit pumping through the <br /> slick-line. The higher water/cement ratio was used when filling <br /> the top of the form to facilitate complete filling of the <br /> bulkhead form. <br /> All-in-all the bulkhead filling proceeded with a minimum of <br /> problems, certainly fewer than I anticipated. The bulkhead <br /> filling produced a bulkhead that should exceed all <br /> specifications. The 28-day strength tests should verify that the <br /> first F-Level/Brenneman bulkhead exceeds all design strength <br /> specifications. <br /> I hope this review of filling the first bulkhead meets your <br /> requirements. <br /> Sincerely, <br /> -4 , d14S .. <br /> John F. Abel, Jr. <br /> Colorado P.E. 5642 <br />