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2012-01-06_PERMIT FILE - C1982057 (34)
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2012-01-06_PERMIT FILE - C1982057 (34)
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Last modified
8/24/2016 4:47:13 PM
Creation date
3/7/2012 7:46:23 AM
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Template:
DRMS Permit Index
Permit No
C1982057
IBM Index Class Name
Permit File
Doc Date
1/6/2012
Section_Exhibit Name
TAB 14 BLASTING
Media Type
D
Archive
No
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<br />• OIL WELL SITE BLASTING <br />SENE CA 1!-W <br />Colorado Cessation Order (CO) No. C-93-141 was issued to Peabody Western Coel Company <br />(PWCC) on October 16, 1993. Abatement step number two states: <br />"Submit a revision to the Seneca II-Y permit that will establish maximum <br />allowable ground vibrations from blasting to provide protection from <br />damage to the oil well and holding tanks." <br />Vibra-Tech Engineers, Inc. was contacted to address the above abatement plan requirement. <br />This firm has been processing and evaluating seismograph is date from the Seneca II-W Nine <br />since operations began. Vibra-Tech's response provides references and related <br />documentation that affirms engineered structures such as wells and tanks can withstand <br />peak particle velocities of at least five inches-pe r-second (ips). Their response to PWCC <br />is attached. <br />PWCC will continue to maintain peak particle velocities at the well site of five ips or <br />• less, and will continue to utilize a seismic monitor at the well site to verify compliance <br />with the five ips maximum limit. <br />Of more importance, is the reason why fly rock occurred. The cast blest that created the <br />fly rock which caused damage to en oil well facility at Seneca II-W was investigated by <br />Peabody Western management. The consensus of opinion is that fly rock was caused by an <br />unknown mud slip or void within the solid strata which was being Last. The mud void was <br />not of competent nature to contain the energy intended to fragment the solid strata <br />typically encountered in this area. Solid competent strata were present in the face of <br />this particular shot. The presence of this suspected void could not have been detected <br />when inspecting the face, nor was it identified when analyzing core drill holes. <br />To prevent a reoccurrence of this event, PWCC proposes to increase bore hale column stem <br />in areas where mud seams are encountered in upper strata. The powder column will be <br />contained in the solid strata and the hole will be stemmed throughout any mud seams. Stem <br />height has been historically set at 23 feet in this pit area, which is substantially <br />greater than the 17 to 18-foot stem height normally associated with 10-5/8•inch drills, <br />• but will be increased as dictated by the depth of the mud. When mud in the upper strata <br />is more than 35 percent of the Cotal hole depth, test holes will periodically be drilled <br />1 Revised 10/26/93 <br />
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