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Mechanical Integrity Test <br />Tubing/Casing Annulus PressureTest <br />U.S. Environmental Protection Agency <br />Underground Injection Control Program <br />999 18" Street, Suite 200 Denver, CO 80202-2466 <br />EPA Witness: No Witness Date: 8 / 17 / 2010 <br />Test conducted by: Adler Hot Oil Service, Inc. (Mike Siepert) <br />Others present: Daren Palmer (Tu & Frum Water) Celina Akin (Solvay) <br />Well Name: 29-26 (C03858-04573) Type: ER SWD Nahcolite Status: AC ® UC <br />Field: Central Piceance Creek Basin <br />Location: 110' S & 1425'W NE Corner Sec: 29 T1 S R 97 W 6th PM County: Rio Blanco State: CO <br />Operator: American Soda. L. L. P. dba Solvay Chemicals Inc. (2717 County Road 215, Parachute CO) <br />Last MIT: 9 / 10 / 2008 Maximum Allowable Pressure: 1000 PSIG <br />Regularly scheduled test? [ ] Yes [ ] No <br />Initial test for permit? [ ] Yes [ ] No <br />Test after well rework? [ ] Yes [ ] No <br />Well iniectinq during test? If Yes, rate: Not iniectinq 0 bpd <br />Pre-test annulus pressure: 0 psiq <br />MIT DATA TABLE Test #1 Test #2 Test #3 <br />TUBING PRESSURE RECORD <br />Initial Pressure N/A psig N/A psig N/A psig <br />End of test pressure N/A psig N/A psig N/A psig <br />CASING/TUBING ANNULUS PRESSURE RECORD <br /> 7" SHORT STRING 7" LONG STRING <br />0 minutes 370 psig 380 psig N/A <br />psig <br />5 minutes 368 psig 379 psig N/A psi g <br />10 minutes 366 psig 378 psig N/A psig <br />15 minutes 364 psig 376 psig N/A psig <br />20 minutes 362 psig 374 psig N/A psig <br />25 minutes 360 psig 372 psig N/A psig <br />30 minutes 358 psig 370 psig N/A psig <br />minutes N/A psig N/A <br />psig <br />N/A <br />psig.. <br />minutes N/A psig N/A psig N/A psi <br />RESULT [?1 ] Pass ( ]Fail [?l ] Pass []Fail (] Pass [ ]Fail <br />Page 1 of 2