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2009-12-21_REVISION - M1980244 (28)
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2009-12-21_REVISION - M1980244 (28)
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Last modified
6/15/2021 5:52:23 PM
Creation date
12/30/2009 8:52:39 AM
Metadata
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Template:
DRMS Permit Index
Permit No
M1980244
IBM Index Class Name
REVISION
Doc Date
12/21/2009
Doc Name
QA Liner Recertification, Monitoring and Test results,
From
CC&V
To
DRMS
Type & Sequence
AM9
Media Type
D
Archive
No
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Cripple Creek & Victor Gold Mining Company <br />Cresson Project <br />Quality Assurance Monitoring and Test Results <br />Liner Recertification <br />December 17, 2009 <br />0 A. a e <br />L 11 , <br />seams prior to the beginning of each day's seaming operation and in the event that devices <br />were disconnected from power and re- energized. <br />Lonestar cut 1 -inch wide samples (coupons) from each trial seam and tested the coupons with a <br />field tensiometer. Lonestar tested each double wedge fusion trial seam twice for peel adhesion <br />(peel) and once for bonded seam strength (shear). Lonestar conducted peel tests on fusion <br />welds on both the inner and outer tracks of each peel coupon. Lonestar tested each extrusion <br />trial seam twice for peel and once for shear. <br />AMEC personnel observed the testing of trial seam samples and documented test results. <br />AMEC observed the tensile testing of each trial seam coupon to verify that project yield <br />strengths were met during shear testing and that failure did not occur in the weld during peel <br />testing. When trial seams did not meet specifications, AMEC verified that the welding apparatus <br />was not used until two consecutive trial seams performed by the same technician /apparatus <br />combination met specifications. The trial seam test results for fusion seaming are presented in <br />Appendix 1 -2. Lonestar used one tensiometer during the project. Figures 2 and 3 show the <br />codes used to designate passing and failing test results. <br />6.1.3.2 Seaming Observations <br />AMEC personnel observed seams before, during and after welding. AMEC checked each seam <br />for adequate overlap prior to seaming and to verify that the seam area was clean and dry. <br />AMEC documented Lonestar personnel performing the seaming and the seaming equipment <br />used. Following the completion of seaming and routine repairs, AMEC checked the full length <br />of each seam to verify that no additional repairs were required. In the event that additional <br />repairs were needed, AMEC marked the location requiring repair on the geomembrane, <br />documented the location, and brought the repair area to the attention of Lonestar. Once <br />Lonestar made repairs, AMEC checked the repair location to verify completion to project <br />specifications. AMEC inspected all seams for quality and completion. AMEC personnel <br />conducted a final walk- through to verify completion of the entire geomembrane system and to <br />identify any additional damage that may have occurred during construction operations. Any <br />additional damage found during the final walk through was marked and documented by AMEC <br />and brought to the attention of Lonestar and repaired. <br />6.1.4 Defect and Repair Observations <br />AMEC inspected geomembrane panels for damage that may have occurred during <br />manufacture, transport, deployment, or installation as discussed in Section 5. AMEC repeatedly <br />observed all panels and seams for defects until Ames covered the geomembrane with DCF. No <br />damaged or defective liner was used. <br />• <br />SAPROJECTS \1125E CCV COA\H2 - DESIGN\LINER RECERTIFICATION REPORT\REPORT BODY\OA MONTIORING AND TEST RESULTS LINER 19 <br />RECERTIFICATION.DOC <br />
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