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Spoil Fill #8, <br />March 10, 2009 <br />Page 2 <br />FILL PLACEMENT <br />Fill placement has been completed in accordance with the approved plan. No additional fill placement is <br />anticipated. <br />COVER MATERIAL <br />Final fill configuration has been established and topsoil material has been placed on the excess spoil-fill. <br />The area was mulched and seeded in the fourth quarter of 2003. Soil was placed and spread on the upper <br />most surface of the fill in May of 2004. During the second quarter of 2005, areas disturbed by maintenance <br />of the armored down-drains were seeded using certified weed free straw and the approved rangeland seed <br />mix. The construction access road east of the east down-drain was hand mulched and seeded during August <br />of 2006. <br />STRUCTURAL INTEGRITY <br />The entire excess spoil fill facility was examined for signs of failure and instability such as tension cracks, <br />ground movement, springs and seeps, and standing water. No indication of potential instability was <br />observed. <br />DOCUMENTATION AND OTHER OBSERVATIONS <br />Spring conditions prevail. Ground conditions are good with fair soil moisture due to the north facing slope <br />of the spoil fill. Both down-drains experienced some damage from August storm events. Operator has <br />completed most repairs on the down drains; but erosion damage remains to be repaired on the upper west <br />lateral ditch. Overall, site is in good condition except as noted. <br />CERTIFICATION <br />This inspection was conducted by Ronald G. Thompson, a qualified professional and MSHA certified <br />inspector of earth and rockfill embankments and impoundments, under the direction of Mr. Charles <br />McGlothlin, a registered professional engineer licensed in the State of Colorado. <br />This is to certify, to the best of my knowledge and belief; that Fill No. 8 construction and placement, as <br />noted since the previous certification and as determined during this inspection and discussions with mine <br />personnel, is in accordance with designs as proposed by CTL Thompson in their report dated April 27 and <br />amended July 27, 2001 and as approved by the Division of Minerals and Geology. <br />a/I <br />Ronald G. Thompson <br />Inspector <br />n <br />r <br />J09 les W. McGlothlin ,-? <br />Professional Engineer