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Project: ......................... ........ ...... ..._.......................... ...; <br />• - GEOTECH <br />J: <br />............................................................................. Client / On Site Rep: <br /> <br />Bowie Resources / B. Bear <br />Bowie Mine Gob Pile Stability ................. I...-..""' - ..................................................... <br />Civil, Structural & Geotechnical Engineers <br />222 South Park Ave <br />• Montrose <br />CO 81401 Contractor / Rep: <br />Load Out Services / Ty Hyatt <br />Project No: <br />2005126-CMT Date: <br />4/8/2009 , <br />. <br />Ph.: (970) 249-6828 - FAX: (970) 249-0945 <br />CONSTRUCTION MATERIALS TESTING LABORATORY Technician: <br />L. Sanchez <br />DAILY CO MPACTION REPORT <br />TES LOCATION TEST TYPE MAX DRY OPTIMUM DRY MOISTURE PERCENT NOT SOIL LAB SAMPLE <br />T <br />NUMBER <br />Embankment Gob - Gob Pile No. 2, Slope Embankment GRADE ELEV NUC SAND DENSITY <br />(pcf) MOISTURE <br />CONT. (%) DENSITY <br />(pcf) CONTENT <br />(%) COMPACTION wrTHlN <br />SPEC TYPE NUMBER <br />257 1D-r#430-)N i 0A-)7 n7 /C -MQ7 O'7 <br />ii.4?r?i 3i nn n <br />61V?.7 v n n' n <br />7V.V in i <br />LV..L n9 11 <br />7G.L t <br />16.1 nn t <br />77.1 1. <br />i3.ob <br />#2213&22y t/(. I-WW 17A <br />258 (PT#4393) N19483.67/E37476,27 6110.7 X 97.1 10.2 96.0 14.1 98.9 gob #228 & 229 r/C 0 1S% <br />259 (PT#4394) N19474.08/E37394.16 6110.8 X 96.8 10.2 98.5 16.1 101.8 gob #228 & 229 r/c @ 14° <br /> <br /> <br /> <br /> <br /> <br /> <br /> <br /> <br />MOISTURE / DENSITY SPECIFICATIONS OBSE RVATION / TESTING FIELD OBSERVATIONS <br />Specified Date: Compaction Equipment Used: <br />Compaction 90%+ Cohesive Soils X <br />Requirement: Cohesionless Soils Full -rime: Day: S M T W <br />X Th F S <br />Sheepsfoot: ?X <br /> Part Time: Weather: Sun Clear Overcast Rain Snow <br />Specified x X Smooth Drum Roller: <br />Moisture /A Cohesive Soils X <br />Requirement: Cohesionless Soils Number of Site Visits/Day: .-?1- _ Temp: To 32 32-50 <br />X 50.70 <br />X 70-8S 85 Up <br />Vibratory: <br /> Testing Only: Wind: Still Mod High <br /> Requested By (Company Name): X X Other (List Below): <br />Laboratory Testing <br />Procedure: ASTM-698 Cohesive Soils X <br />Cohesionless Soils <br />Ty Hyatt / Load Out Services <br />Humidity: <br />Dry <br />X <br />Mod <br />Humid <br />Haul Traffic <br />DENSITY / COMPACTION TESTING WAS NOT PERFORMED <br />ON THIS DATE FOR THE FOLLOWING REASONS: Insufficient amount <br />lof material placed. Informed (Rep of Company) of Test Results: <br />Ty Hyatt /Load Out Services <br />Buckhorn was not informed prior <br />Contractor Not Working Due To: The Contractor Is: to our arrival on site that the <br />contractor would not be workin <br /> <br /> <br />Inclement Weather: <br /> <br />Equipment Malfunction: <br /> <br />Processing Frozen Material: =Processing Wet Material: <br /> <br />Stripping and/or Grubbing: Moisture Conditioning Dry MaYI: <br />Field Copies Given To: <br /> <br />Contractor: <br />Client: g <br />on this date. <br /> <br />Unknown: <br />stockpiling Fill; =Removing Unsuitable Mafl: CM/GM: <br />Other: PAGE 1 OF 1 <br />05-126-CMT Bowie Mine Gob Pile Stability.xls DCR4-8-091s#257-aa