My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
2008-07-11_PERMIT FILE - M2007044 (7)
DRMS
>
Day Forward
>
Permit File
>
Minerals
>
M2007044
>
2008-07-11_PERMIT FILE - M2007044 (7)
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
8/24/2016 3:34:32 PM
Creation date
7/17/2008 8:25:07 AM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M2007044
IBM Index Class Name
PERMIT FILE
Doc Date
7/11/2008
Doc Name
Appendix J, K, and L (volume 2)
From
Energy Fuels Resources Corp
To
DRMS
Email Name
GRM
Media Type
D
Archive
No
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
104
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
CTLITHOMPSON <br />January 14, 2008 <br />Greg Lewicki and Associates <br />11541 Warrington Court <br />Parker, Colorado 80138 <br />Attention: Mr. Ryan Ellis <br />Subject: Rock Core Test Results <br />Project No. CT14431-455 <br />Dear Mr. Ellis: <br />This report presents compressive strength and permeability results for a rock slab <br />that was delivered to our laboratory. The rock slab was cored and samples were <br />prepared for compressive strength and permeability testing. <br />The rock core was tested in general conformance with ASTM D 7012 (Method C), <br />"Compressive Strength and Elastic Moduli of Intact Rock Core Specimens under Varying <br />States of Stress and Temperatures." The sample did not meet the specification the height <br />to diameter ratio, due to the size of the original specimen. The compressive strength of <br />the core is 9,050 psi. To correct for the shorter than specified height to diameter ratio we <br />applied a correction factor according to ASTM C 42 for concrete cores. The correction <br />factor for the height to diameter ratio is 0.938 which is equivalent to a corrected <br />compressive strength of 8,490 psi. Results are presented in Table 1 <br />One 3-inch diameter core was submitted to Knight Piesold for permeability testing <br />using a flex-wall permeability (ASTM D 5084). The permeability of the specimen is 2.9 x <br />10-5 cm/s flow for the 3-inch diameter core. <br />The hydraulic conductivity test (USBR 5600) is currently running on an 8-inch <br />diameter core. The very low permeability makes this test very slow, and as of now, no <br />flow has been detected in the test method. After flow begins, data can be taken and we <br />will send the results of the testing when the testing is complete. <br />If you have any questions regarding the information in this report, please feel free <br />to contact us. <br />Respectfully submitted, <br />CTL I THOMPSON MATERIALS ENGINEERS, INC. <br />Matthew A. Best/ <br />Materials Lab Manager <br />Reviewed by: <br />Awl /el, 1 . <br />Orville R. Werner II, P.E. <br />Principal <br />MAB:ORW/mab <br />22 Lipan Street I Denver, Colorado 80223 1 Telephone: 303-825-0777 Fax: 303-893-1568 <br />This test report relates only to the items tested and shall not be reproduced, except in full, without written approval of CTL Thompson, Inc.
The URL can be used to link to this page
Your browser does not support the video tag.