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REP38253
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REP38253
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Entry Properties
Last modified
8/25/2016 12:19:04 AM
Creation date
11/27/2007 8:01:41 AM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
C1981012
IBM Index Class Name
Report
Doc Date
5/20/1993
Doc Name
REFUSE DISPOSAL AREA NEW ELK MINE LAS ANMIAS COUNTY COLO JOB 20,122
From
CTL THOMPSON INC
To
BASIN RESOURCES INC
Permit Index Doc Type
STABILITY REPORT
Media Type
D
Archive
No
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During our site visits, we have observed exposed portions of the underdrain extending <br />up the two drainages beyond the limits of refuse till. We were provided photographs from <br />1991 and 1993 (Fig. 1) which show the drain extending above the fill present at the time <br />of each photo. These photos and our Bile observations ;ndiCaie ii,0 drain has been <br />installed in substantial conformance with the approved plan. <br />We have no knowledge whether the keyway cut planned at the base of the pile was <br />installed. If you have records regarding the keyway installation, we can review them. <br />Compaction and stability of the refuse was the focus of our investigation in 1991. We <br />have enclosed a copy of our 1991 report for MLRD reference. In general, our <br />investigations have indicated compaction of the refuse fill has generally achieved 80 to <br />100 percent of maximum ASTM 0698 dry density. We have reviewed compaction test <br />data by Lincoln-Devore, Inc. for testing which occurred September 30, 1987. In addition, <br />we performed additional tests in May 1993. The Lincoln-Devore tests showed 77 to i 00+ <br />percent compaction and our recent tests indicate 89 to 100+ percent compaction in the <br />top poRion of the fill (Appendix A). In general, we do not feel the planned 90% <br />compaction criteria has been met for the refuse fill. During our 1991 study, we found the <br />stability of the refuse slope to be comparatively insensitive to material density. Our <br />analyses showed the refuse till exceeds required factors of safety for slope stability. We <br />recommended measures to lower moisture content of the refuse materials to enhance <br />stability. Basin Resources has taken measures 20 achieve lower moisture as described <br />in our letter of May 3, 1993. These measures have apparently also enhanced the <br />workability of the materials (that is, the ease of compaction) as indicated by our recent <br />compaction tests. <br />MLRD requested we provide an opinion of the acceptability of the "dirt" and rock materials <br />which have been placed in isolated, wet areas of the fill surface to allow equipment <br />access. MLRD personnel indicated large rock fragments (up to six feet) have been <br />observed. In our opinion, the placement of these materials in the refuse pile is acceptable <br />and does not significantly influence slope stability of the facility. We have not found <br />documentation that placement of the materials in the fill was part of the approved plan. <br />It is not necessary to remove the materials from the fill iron a geotechnical perspective. <br />We reiterate that surface drainage should be maintained to reduce the need for use of <br />these materials. <br />Section 4.09.1 (11) requires inspection of the fill for stability by a registered engineer. Our <br />Mr. McOmber has observed the fill in 199t and in April 1993. During our site visits we <br />have found no appearance of instability, structural weakness, or other hazardous <br />condition. On the basis of our review of conditions at the facility in 1991 and 7993, our <br />analyses and review of the limited available data, we believe the Refuse Disposal Area <br />has been constructed in substantial accordance with the design approved by the Mined <br />Land Reclamation Division with the exception of compaction of the existing materials and <br />maintenance of the crown on the temporary fill surface. We believe the degree of <br />compaction achieved to date is adequate to ensure stability of the fill. Process changes <br />adopted since 1991 will further enhance stability. We recommend surface drainage on <br />the temporary fill surface be re-established as soon as practical when placement resumes. <br />3 <br />
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