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REP16554
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REP16554
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Entry Properties
Last modified
8/24/2016 11:45:49 PM
Creation date
11/27/2007 1:55:01 AM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1999002
IBM Index Class Name
Report
Doc Date
8/5/2004
Doc Name
Plugging and Abandonment of Wells & Reports
From
American Soda LLP
To
DMG
Media Type
D
Archive
No
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Form 3160-5 UNITED STATES eoaM nPPnovso <br />Qune 1990) DEPARTMENT OF THE INTERIOR Budget Bureau NwlgM-0135 <br /> Ex ~ MvN31, 19Xi <br />BUREAU OF LAND MANAGEMENT 5. IE•ee oesign•aon ud Serie] Nw <br />SUNDRY NOTICES AND REPOR75 ON WELLS Yankee Gulch CC)118328 <br />Do not use this form for proposals to drill or to deepen or reentry to a different reservoir. s. ut,m~•.~, Auou•• or Trae Name <br />Use "APPLICATION FOR PERMIT-" for such ro N/A <br />SUBMIT II4 TRIPLICATE r. uuna •rcA, ng,eemem ee"g1ebOn <br /> NA <br />1. Type of Well & Well NameeM Nw <br />^ Oil Well O Gas Well ®Chher Nahcolite Solution Minin 20.14 <br />2. Name of Operator s. API WeB Nw <br />American Soda, L.L.P. <br />3. Address and Telephone No. ro. Puld...d Pml, m B.pl"remy Area <br />2?17 C . Rd. 215 Parachute, CO 81635 970 2B.5.6500 Central Piceance Creek Basin <br />4. Location of Well (Footage, Sec., T., R., M., or Survey Description) 11. Cowuy m Peri•h, 5tme <br />Basting and Northing NB ~/i of SE'/i of Section 20, TIS, R97W 6d P.M. Rio Blanco, CO <br />N 13661.06 <br />E 14987.09 <br />12. CHECK APPROPRIATE BOX(s) TO INDICATE NATURE OF NOTICE, REPORT OR OTHER DATA <br />TYPE OF SUBMLSSION TYPE OF ACTION <br />^ Notice of Intent ®Abandonment ^ Change of Plans <br /> ^ RerompleEOn ^ New Construction <br />^ Subsequent Reports ^ Plugging Back ^Nun-Routine Fracturing <br /> ^ Casing Repair ^ Water Shut-0ff <br />®Final Abandonment Notice ^ Altering Casing ^ Conversion to Injection <br /> Ckher. ^ Dispose Water <br /> Mote Bepon.e•mmm•mpu~pau®~wm <br />13. O®MROpmed mCmnplmd Opmti~([]aay mteNpvaoevtdttaat a•d give pvtivmtNm. including et®e imeedsatiu6~1 P^P^+d wads awAvtluvtimaDy dvLM qK Vhodae laan®v <br />and mafart i and tlve vvtiral deplN Ira s0 wbaa ad rmn petlvml m the w~i' <br />Dissolution surface at 1442'. <br />4/1/2(101 Rig up Key Energy. <br />4/2/2IXf} Pub 2202' of 4'/z' long string. Gauge ring stopped at 1381'. <br />4/3/2004 PuB 164T of 4'h" short string. Gauge ring stopped at 1391'. <br />4/14/2004 Attempted to set 4lh" cement basket into short T' using, stopped at 1450. Pulled cement basket out of casing. <br />4/22/2004 Tripped into short string 7" casing with 5 7/8" bit to 1467 and leaned [01490' <br />4/23/2004 Tripped into long string 7" casing with 5 7/8" bit and leaned to 1494. <br />4/26/2004 Ran Gauge rigs on both T' casings, could not get past 1390'. Cleaned out [01490' on T' long string w 61/8" bit. <br />4/27/2004 Cleaned out T' long string with 6 7/8" mill to a reported depth of 1480', twisted off 6/18" mill and connecting sub. <br />4/28/2004 Cleaned out T' short string with 61/8" mill to a depth 7490'. <br />4/29/2004 Ran gauge rings down both T' using strings, rould not get gauge rings past 1390'. Attempted to nm 2 7/8 mment basket into <br />T' long string casing. Basket stopped at 1401'. <br />4/30/2004 Cleaned out T' long string with 61/8" mill to a reported depth of 1470'. <br />5/3/2004 Ran 2 7/8" basket in both short and long T' casirSgs to a reported depth of 1470'. Cemented with 5 sacks of cement on each <br />basket. <br />5/4/2001 Backed off baskets in both casings. Long string 7" casing began to Eow at surface. (Please reference undesirable event report) <br />5/10/2004 Pumped 10 sacks of cement on short string T' casing. <br />5/11/2004 Pulled 2 7/8" string from long string 7" casing and discovered [hat the cement basket remained attached. <br />5/12/2004 Tripped into long string 7" with 2 7/8" tubing string. Tubing stopped at 1441. <br />5/28/2004 Tripped in long string T' with impression block to 1441'. <br />6/1/2004 Tripped in long T' rasing with fishing tool assembly, mold not get past 1398'. <br />6/2/2004 Tripped in long T' casing with 61/8" swedge, mold not get past 1398. Tripped in with 54'd" swedge, mold not get past 1414' <br />6/3/2004 Performed downhole camera and caliper survey on both strings. The downhole mmem indicated that both casings were parted at <br />1394'. <br />6/17/2004 Cudd Pressure Conuol attemped to run mil tubing into 7" long string casing. The coil tubing stopped at 1391' -1394'. <br />7/ 6/2004 Tripped 2 7/ 8" tubing to 1440' on T' long string casing. Tripped 27/8" tubing to 1447 on T' short string using. <br />7/7/2061 Pumped 25 sacks of SO% Type G cement and 20% Bentonite on T' long string casing with 2 7/S" tubing at 1440'. <br />7/7/2004 Ran into T' short string and stopped high 4sJ 1396'. <br />7/7/2004 Ran into 7" long string and tagged cement ®1430'. <br />
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