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Form 37605 UNITED STATES FORM APPROVED <br />Qvne ]990) DEPARTMINT OF THE INTERIOR Budget Bureau Na lOB4-0135 <br /> Ez ~ues Mvch31, 1996 <br />BUREAU OF LAND MANAGEMENT s. Leese Dag,,.uva °~a serial Nw <br /> Yankce Gulch CO-118325 <br />SUNDRY NOTICES AND REPORTS ON WELLS <br />Do not use this form for proposals to drill or to deepen or reentry to a different reservoir. e u irdiew Auon« or rr3e Nerve <br />Use "APPLICATION FOR PERMIT-" for such N/A <br />SUBMIT IN TRIPLICATE r- Ir u,w «cA, Agre~mt Dmignetion <br /> A <br />1. Type of Well s, weu N®ne.w Nw <br />^ Oil Well O Gas Well ®Other Nahcolite Solution Minin American Soda LLP T43 <br />2 Name of Operator 9. API Well Nw <br />American Soda, LLP. <br />3. Address and Telephone No, la FvM eaa Pmt m e~PI°~°'°~5' AR° <br />2717 C . Rd. 215 Parachute, CO 81635 970 285bS00 Central Piceance Creek Basin <br />4. Location of WeB (Footage, Sec., T., R., M., or Survey Description) Il. CouMy or Push, State <br />B 14,382 N 13,928 NE'/i of 5E r/i of Section 20, TIS, R97W (>'s P.M. Rio Blanco, CO <br />12. CHECK APPROPRIATE BOX(s) TO INDICATE NATURE OF NOTICE, REPORT OR OTHER DATA <br />^ Notice of Intent <br />ACTION <br />^ Subsequent Reports <br />®Final Abandonment Notice <br />® Abandonment <br />^ Recompletion <br />O Plugging Back <br />^ Casing Repair <br />O Altering Casing <br />Other. <br />^ Change of Plans <br />^ New Constmction <br />^ Non-Routine Fracturing <br />^ Water Shut-Off <br />^ Conversion to Injection <br />^ Dispose Water <br />Mar Repoam°lammvltipe,mpleummwm <br />13 nuu0e ROpmei u~CmP4redOpmtiom(Omi9 waoea0 pawmraavl; mdgieepaWm~dne.arl^N^&a®aeertmielwvmB mr P^P^~~~aweaia'varmaay JErM,9re mbnd°ce lrcati® <br />ma msaveamamu.nerzlhpbbaow~tn+®a,mvp+temtmaa,.vcY <br />WeB 203 dissolution surface at 1401'. <br />4/15/04 Rig up Key Energy on weB and mt 2 7/8" tubing at 1544. <br />4/16/01 fulled 1544' of 27/8" tubing. <br />4/19/04 Cut 4'h" pipe at 1544'. Pulled 1544' of 4th" tubing from well. Ran ring gauge. Ring gauge stopped at 1355'. <br />4/20/04 Ran mill and rollars into well, milled to 1371'. Tripped out of hole. <br />4/21/04 Ran in well with 5 7/8" bit and cleaned to 154T. Tripped out of hole. Set cast iron bridge plug at 1543,5. Rigged down Key Energy. <br />6/17/04 Cudd Pressure Control Mpped to 1539 feet with mil tubing unit into rombmation 9 5/8" by 7" °S1 t8 string. Halhburton pumped <br />400 sacks of 15.6 #/gal Type G, 35% SSA, 0.2% CFR3 neat cement and displaced mil tubing with water. (Please reference ASLLP Plugging <br />and Long Term Standby Summary) <br />7/7/04 Stewart Welding cutoff wellhead caPP~ 9 5/8" casing, and labeled cap. <br />14. I hereby certify that the foregoing <br />Signed <br />(This space for Federal or State office use) <br />Approved by <br />Conditions of approval, 0 any: <br />Title 18 U.S.C. Section 1001, makes it a Qime for any person knowingly and willfully to make to any department or agency of [he United <br />States any false, fictitious or fraudulatt statements or representations as to any matter within its jurisdiction. <br />