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The auxiliary ditch has been designed to convey flows generated by the Probable <br />Maximum Thunder Storm. These flows were calculated by Charles F. Leaf in <br />March, 1978. As indicated in this report a high point exists in the diversion <br />channel with the flow being directed in both directions around the surface <br />facilities. The auxiliary diversion ditch recommended herein would follow this <br />general pattern. Access across this ditch would be provided at the high point and <br />just east of the fan. <br />The auxiliary diversion ditch, as it is located on the fan level proper, will collect <br />disturbed flows generated on the bench as well as upstream flows introduced by a <br />faffure of the primary diversion ditch. A small culvert will be provided to <br />reintroduce disturbed flows to the original drainage system on the east end of the <br />fan level. Flows in excess of these flows will be directed into the original <br />diversion ditch. The diversion structure will consist of a 21 inch CMP culvert and <br />a concrete weir. The culvert will pass all minor flows without bypassing the <br />sediment control system. The concrete weir will be overtopped only when flows in <br />the auxiliary diversion ditch exceed the minor system design flow of 13 efs. Very <br />little disturbed flow will enter the auxiliary ditch which flows west, consequently <br />no separation method will be provided. <br />PORTAL BENCH: <br />Some problems with drainage clearly exist on the portal level; however, according <br />to Geo-Hydro Consulting, they appear to have only a limited affect on the <br />stability of this fill. <br />• The ditch on the upstream side of the access road above the portal bench diverts <br />flow around the bench. This ditch is constructed at the same grade as the access <br />road. <br />The swale to the west of the bathhouse is virtually non-existent. The area in the <br />vicinity of the ditch was saturated at the time of the site visit, on October 28, <br />1981. This ditch should be re-established to prevent saturation of this area. The <br />ditch should be regraded to drain to the south to Node 4, as shown on the surface <br />facilities drawing. This will alter the original drainage pattern by redirecting flow <br />generated west of the bathhouse from Pond 1 to Ponds 3 & 4. We feel the flow <br />should be discharged from the fill as quickly as possible to prevent any possible <br />saturation problems. <br />The other swales on the portal bench are not well defined; however, the ditches <br />and the bench in their vicinity are paved and therefore should prevent saturation <br />of the f~11. <br />SUBSTATION FILL AND TRANSFER TOWER iil FILL: <br />After having reviewed this with Geo-Hydro Consulting, we feel there are no <br />drainage related stability problems associated with these fill areas. <br /> <br /> <br />