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~: <br /> <br />As shown in the Espey, Huston 8 Associates report (page c-34a and <br />appendix R of the permit application) the 1JotF~ern No. 1 Sedimentation <br />Pond is designed to contain the 10 Year-24 hour storm. Also the <br />spillway was designed to Safely pass the 25 year-24 hour event. <br />The amount the 1,- inch gated spillway on the Northern No. 1 <br />Sedimentation Pond r...:-t be opened to allow for automat lc deuatering <br />with an average rEi•_~:ion time of 24 hours is 2 inches (see attached <br />calculations). <br />FF'F rC OISPOSA - RR R FOND <br />• <br />`J <br />Rs shown fn the Es.p ey, Huston b Associates report (pages 13-11 and <br />13-52 of the mine per-~n~t application) the F,•~fuse Disposal Sedimentation <br />Pond is designed to cc•-.tain the 10 year-~-l hour storm. Also the <br />sp SllwaY was designed to safely pass the ~. •~~e ar-24 hour event. <br />The Refuse Disposal ~,rcr wand has an opera <br />This pond was evid Exit ];• designed to <br />average retention tirc~~ of 24 hours. The <br />maintain an average retention time of 24 <br />second (see attachetl calculations). The . <br />inch iron pipe using the Haz in-Wi11iaR~ F~ <br />cubic feet per second (see attached calci~ <br />an average retention time of approximatEi. <br />inch iron outlet pipe. <br />~ticaly dewater with an <br />tity of flow required to <br />is 0.84 cubic feet per <br />:r,~Vm flow through the 6 <br />la was found to be 0.74 <br />.`ons). Therefore providing <br />hio urs. <br />As shown in Rppendix ^-2R3 & 4, Modific<~ ~,~ No. 2 of the permit <br />application and the Panorama Resource Ser•c~:~rs report of Rugust 1, 1984 <br />the Sedimentation Pond A was constructed tc• r.ontain in excess of a 10 <br />year-24 hour event. Also the spillway was _=_ianed to pass safely the <br />25 year-24 hour event. <br />The amount the 12 inch gated spillway on the Rienau No. 2 Sedimentation <br />Pond A rrK+st be opened to allow for automatic dewater ing with an average <br />retention period of 24 hours is 1.5 inches (See attached calculations). <br />