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FIG. 9 <br />It <br />e <br />~n <br />~n <br />~0 <br />is <br />;i <br />Gateroad conveyor profile. Conveyor system design was the most challenging part of the long panel longwall design at <br />Twentymile. <br />HEAD <br />6000 ~2~ <br />ssao <br />9 RIGHT PROFILE <br />°o p <br />0 0 <br />_........o _ <br />0 <br />0 <br />0 <br />manufacturers were chosen to provide samples for test- <br />ing. Both belting designs passed the tests performed on <br />dynamic testing equipment in Germany. So the decision <br />became a mattzr of economics. <br />The ability to provide a 3.8-MPa (2,000-psi width) <br />belt then led to the design requirements for the equip- <br />ment that would kzep the tension constant in [he system <br />and limit the number of trippec drive installations. TCC <br />had several years of expzrience with tripper drive instal- <br />lations- in the western mining district and felt comfort- <br />able continuing that in the EMD. <br />The major difference between the western and east- <br />ern mining districts was the use of power trippers in the <br />west and the combination of powering and braking/re- <br />generative trippers in the east. The control systems and <br />software necessary to allow the various drives in the long <br />panel belt to keep [he tension constant was performed <br />between TCC and a leading conveyor manufacturer. <br />The conveyor would also require a tail braking sys- <br />tem as part of the total package. This tail brake was in- <br />corporated into the longwall tailpiece after hours of <br />engineering collaboration between [he mine and the <br />conveyor manufacturer. The system has worked well <br />throughout [he first two long panels of the district, al- <br />though alignment issues in the first panel required some <br />redesign. <br />Another unique portion of the total conveyor sys- <br />tem is the collapsible structure used for 76 m (250 ft) <br />between the longwall stageloader and the rigid structure <br />installed on development. This system has provided im- <br />proved productivity because [he longwall crews do no[ <br />have to pull belt structure on retreat. <br />There were many interrelated conveyance issues to <br />provide a successful single-flight conveyor system that <br />would handle 4.5 k[/h (5,000 stph) and 6,700 m (22,000 <br />ft) and be engineered in the required timeline. Several <br />are mentioned here but there were other issues that <br />needed to be either engineered or solved by the mine <br />operations personnel. <br />Longwell equipment design <br />The key element in the equipment design for [he <br />longwall in long panels is the 5.4 raw Mt (6 million raw <br />st) of coal mined between longwall moves. TCC began <br />experimenting with equipment life by skipping rebuilds <br />between panels on major components, such as ranging <br />:arms and armored face conveyor gear boxes. The ab- <br />;ence of data in the industry pertaining to long panels <br />:Ind high tonnage before rebuild did not help in the de- <br />cision making. The longwall has mined nearly two long <br />panels to date and the results on equipment life vary due <br />6°~ <br />TAIL <br /> <br />0 0 <br />+ + <br />o <br />u <br />i n <br />to [hz variations in mining conditions. The longwall <br />equipment had to meet the goal of 4.5 kt/h (x.000 stph) <br />capacity. And it had to fit into the seam requirements <br />from 2.13- to 2.74-m (7- to 9-ft) mining height. <br />The shearer speed is capable of 45 m/min (150 fpm) <br />to provide [he 4.5 kt/h (~,D00 stph) capacity in the unique <br />cutting system at TCC. The shearer typically cuts a half <br />web in each direction to control the immediate roof and <br />face bursting. This cutting method lends itself to high <br />shearer speeds because the required cutting force is lim- <br />ited. Thz ergonomics of the longwall shields was scruti- <br />nized because the operators would be traveling an <br />average of 10 km (6.2 miles). per 10-hour shift. The <br />shield capacity and ergonomics design had [o meet the <br />varying geologic paramzters of the EMD and the re- <br />quirements of walkway and head clearance. This was <br />primarily accomplished with large-diameter leg shields. <br />These enabled the shields to provide the setting forces <br />required and adequate walkway clearance. <br />Conclusion <br />Several of the project requirements described here <br />provide a sense of scope for the amount of work and is- <br />sues that needed to be resolved in designing long long- <br />wall panels a[ TCC. A key concept a[ [he beginning of <br />the EMD project was increasing the longwall: continu- <br />ous miner ratio and reducing mine costs. These criteria <br />coupled with the goal of 4.5 kt/h (5,000 stph) led to many <br />of the design considerations used in the long panels. <br />Another important note is that all the issues de- <br />scribed were coordinated while still operating a longwall <br />mine at 2.7 [0 4.5 clean Mt/a (3 [0 5 million clean stpy). <br />Many of the subprojects described had to be worked into <br />the existing mine operations for testing and timely data <br />collection before the EMD would be developed. <br />After the original project engineering was com- <br />pleted, the actual length of panels in [he EMD was 5.488 <br />m (18.000 ft) due to development timing from geologic <br />conditions. This shorter length does not take away from <br />all the issues and engineering design listed here. They <br />have resulted in world record production including 919 <br />kt (1 million clean st) in Lune 1997. <br />The developments of long panels for longwall min- <br />ing at TCC was completed through the efforts of several <br />operations, administrative and engineering personnel at <br />Cyprus Amax Coal, along with many manufacturers and <br />vendors. The long panel project has contributed many <br />new underground longwall mining concepts and prac- <br />tices that have become new standards throughout the <br />world. It has also removed barriers that might otherwise <br />not have bezn tested in the coal mining industry. ^ <br />MINING ENGINEERING ^ DECEMBER 7998 27 <br />