My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
REV09312
DRMS
>
Back File Migration
>
Revision
>
REV09312
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
8/25/2016 1:09:49 AM
Creation date
11/21/2007 10:02:05 AM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1977378
IBM Index Class Name
Revision
Doc Date
2/20/2003
Doc Name
Construction Certification Report
From
Sunnyside Gold Corp
To
DMG
Type & Sequence
TR25
Media Type
D
Archive
No
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
21
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
American Tunnel Bulkhead No.3 <br />Construction Certification Report <br />Page 5 <br />Low aressure troutin~ of the concrete-rock contact <br />After construction of the air-side bulkhead form and placement of rebar, the form was <br />marked for drillhole collars by nailing faucet washers to the form at the selected <br />locations. One ring consisting of nine holes was drilled to intersect the rock contact <br />along the perimeter at approximately the mid-point or center of the bulkhead, The target <br />points were selected and then appropriate corresponding collar points were selected such <br />that the hole could physically be drilled without hitting the rebar mat. Angles and <br />distances were measured so the selected lines could be reproduced after the bulkhead <br />form was stripped. <br />The bulkhead was drilled and the contact was low pressure grouted the week of <br />November 25, 2002. <br />Each hole was pressured to 200+ psi with very little grout take although one series of <br />holes appeazed to take grout into the formation. These holes were re-drilled on successive <br />days and grouted until refusal, <br />The construction pipe was permanently closed on December 3, 2002 and additional <br />formation grouting was done downstream of the bulkhead for the remainder of the week. <br />Very little grout was accepted during this process. <br />Construction Drain Pine Closure <br />The construction drain pipe was permanently grouted closed and capped on December 3, <br />2002. A grout pig was pumped ahead of the grout to separate the water and grout. The <br />catch bars placed in the up-stream end of the pipe provided a stop for the grout pig <br />allowing complete and total filling of the pipe. The valve was closed under pressure to <br />prevent bleed-off. After curing of the grout in the pipe, the valve was removed and a <br />stainless steel blind flange was bolted to the pipe flange. The pipe has been permanently <br />sealed. <br />The American Tunnel Bulkhead No.3 construction meets or exceeds all design <br />specifications. <br /> <br />
The URL can be used to link to this page
Your browser does not support the video tag.