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Summary of Adequacy Review for TR-105 <br />Mine: West Elk Date review completed: 3/15/06 <br />Permit No.: C-SO-007 DMG reviewer: Tom I{aldenbaeh <br /> Require- <br /> ments <br />Requirements complied Comment <br /> with 7 (yes I <br /> no <br />Right of entry <br />yes <br />The operator owns the land. <br />(2.03.6) <br />Cultural resources The proposed work will be within an area previously approved for mine <br />(2.04.4) Yes disturbance in TR-79 (see attached map). Cultural resources cleazance was <br /> obtained in TR-79. <br />Fish/wildlife <br />information (2.04.10, The proposed work will be within an area previously approved for mining <br />2.04.11, 2.05.6(2) yeS disturbance in TR-79. Fish and wildlife cleazance was obtained in TR-79. <br />and 4.18 <br />Maps and plans <br />Yes <br />The submittal includes a PE-certified map. <br />2.10 <br />Topsoil (4.06) and The proposed work will be within an area previously approved for mine <br />topsoil markers disturbance in TR-79. The plan for topsoil salvage for the area was appoved <br />4.02.7 in TR-79. <br /> Runoff from the distubance proposed in TR-105 and runoff from <br /> undisturbed areas uphill from the disturbance will be routed through the two- <br /> cell RPE pond via the temporary RPE ditch. A SEDCAD run in the <br />Water quality submittal indicates the pond will have 1.8 acre-feet of excess capacity with <br />protection (4.05.2) yes the addition of cleaz water diversion ditch DCW-Schas adequate capacity to <br /> treat the runoff Runoff from the disturbed area can be expected to be <br /> alkaline with quality similar to pre-disturbance conditions. The runoff can be <br /> expected to be too alkaline to form leachates or to mobilize metals in the <br /> soils. <br /> Ditches are sized to handle a 100-yeaz storm. Clean water ditch DCW-8A <br /> will divert undisturbed azea runoffto Sylvester Gulch that originates from <br />Small diversions undisturbed areas immediately west and southwest of the disturbed area. <br />(4.05.3) Ditch design capacities were checked with the Manning equation (see <br /> attached spreadsheet). Riprap sizes appeared adequate based on The <br /> SEDCAD runs in the ditch designs used reasonable variables and <br /> azameters. <br />Sediment control The SEDCAD run in the submittal that verified the RPE pond capacity <br />4.05.5 yeS used reasonable variables and arameters. <br />Reclamation plan <br />(2.05.4),backfilling/gr The submittal contains a plan to remove structures, backfill, regrade, and <br />ading (4.14), yeS seed. <br />reve etation (4.15) <br /> Page 3 of the submittal provides for grouting aquifers in the vent shaft that <br />Permanent sealing are not adequately protected by the concrete lining. Pages 4 and 9 of the <br />(4.07.3) yes submittal provide for permanent capping of the RPE shaft with a concrete <br /> and steel structure. Page 11 provides the plugging plan for the two drill <br /> holes. <br /> The proposed shaft and drill holes will be constructed on the hillslope <br />Coal mine waste immediately upslope from the refuse pile. The shaft and drill holes will have <br />banks (2.05.3(8) and yes no impact on the structural stability of the refuse pile because the shaft and <br />4.10) drill holes will not increase surface runoff or underground seepage in the <br /> refuse ile. <br />Bond amount (3.02.2) yes DMG estimates reclamation costs of $19,242 (see attached estimate). <br />