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HYDRO30996
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Entry Properties
Last modified
8/24/2016 8:54:44 PM
Creation date
11/21/2007 1:06:42 AM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
C1989074
IBM Index Class Name
Hydrology
Doc Date
9/20/2004
Doc Name
3rd Qtr 2004 Inspection Report
From
Greg Lewicki and Associates
To
DMG
Permit Index Doc Type
Sediment Pond Inspections
Media Type
D
Archive
No
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Rimrock Mine Sediment Pond Certification <br />The site inspection was conducted on September 11, 2004. It was a sunny mild day of <br />approximately 80 degree temperature during the visit. The site was dry although it <br />appeared that good rainfall had occured since the last inspection since the site was very <br />green. There was no water in the pond or in Engleville Gulch. There were no erosional <br />problems or any other stability problems with the pond and there was no evidence that <br />the recent storm had caused a discharge in the principal spillway. Both spillways were <br />functioning properly. Engleville Gulch was wet at the surface in some areas. Vegetation <br />was adequate on both the inside and outside slopes of the embankment. The pond is to <br />be left as a permanent impoundment for use in the grazing operation. The staff gage in <br />the pond showed 2.0 feet of sediment level and no water above that point. <br />The following items were checked to see. if they coincided with the design shown in <br />the mine permit application. I, Greg Lewicki, did the pond design in March of 1990. <br />1) Constructed Elevations: The elevations listed below were checked with a precision <br />level and stadia rod: <br />-Dewatering pipe inlet <br />-Dewatering pipe outlet <br />-Top of Dam <br />-Bottom of Emergency Spillway <br />-Toe of Dam (outside and inside) <br />-Bottom of Pond <br />-A number of points within the pond <br />All elevations were found to be acceptable. The inlet to the principal spillway was <br />placed at a slightly higher elevation to allow more sediment storage. The 10 year - 24 <br />hour runoff storage was still present above the principal spillway. <br />2) Width of Emer ency Snillway Design: 12 feet. Measured: 12.2 feet. <br />3) Denth of Emergency Spillway Design: 1.55 feet. Measured: 1.60 feet. The spillway <br />showed no evidence of flow or any signs of erosion or other instability. <br />4) Width of top of Dam Design: 10 ft. Measured: 10.2 ft - 10.6 feet. <br />5) Principal Spillway Design: 4.0" pipe placed in compacted embankment. Measured: <br />4" steel pipe placed in compacted embankment. Extensions on this pipe were added to <br />both sides so that the embankment could be widened. Some black plastic hose was also <br />present near the spillway at the time of the inspection but was not functional. The <br />
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