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PERMFILE71003
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PERMFILE71003
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Entry Properties
Last modified
8/24/2016 11:20:20 PM
Creation date
11/20/2007 11:39:31 PM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1999002
IBM Index Class Name
Permit File
Doc Date
6/18/1999
Doc Name
SOLUBLE SALT PROCESSES FOR IN SITU RECOVERY OF HYDROCARBONS FROM OIL SHALE
Media Type
D
Archive
No
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<br />•-. <br />nahretitc with some small ~es of oil ehale, wa dif- <br />eolvtd and circulated acing lresh water through a small <br />continuous wbinP (the 2-Ifl61n. dilution string had not <br />been installed). The atcond plug, which consisted <br />prirrurily of oiLehale pieta that had puled through the <br />#~In. sloa In the 7•in. cuing, required drilling out. <br />Tubing wu pal lod and a wart-wrapped lino wilt l f32-in. <br />slots wu installed on dte irtS,dc of the slotted section of <br />tht 7-in. cuing. Tht 3Yu-in. tubing std 2- I(161n, dilu- <br />tion string war then installed. <br />Phue 11 of the cream ,njeRan-feeovay period darted <br />on May 76 and tonlinued to Lunt 77, 1971. Flow im- <br />paitmen~ wu prutnt from the start, either at the recently <br />insutlcd sheen ar in the ad}atent rubble-ftlld prottts <br />volume. Afteran unsucttasful steamandhot-wataback- <br />Ilush of the production tubing and wiry-wrapped lino, <br />750ga1 of tempmturc•reurded acid woe used. Rtaump- <br />tan of steam tnlection soon met tht tempcraturt obju- <br />tiscs at chctop and bottom of the process volume, Indicat- <br />ing 1hal the acid treatment had been curetsslul <br />First oil produnion wu noted on June 17, and it <br />gndually increazed to 20 H,T) by June 2~. About this <br />nme, the Clow impairment rcoccurrcd, with the pressure <br />behavior indiratiny a down-hose reatnaion garlic in the <br />2-]llbin. tubing or in the annular fpscc between the <br />bottom of this tubing and the top of s',e wire•wnpped <br />doneC hoer. Failurt of the 2l+-m injrcdon tubing whllt <br />rtuidizing the producton eidc uwd the loss of an <br />tStututed 75 bbl of oil. Evaluation of the second acid <br />trutmcnt (2,000 gal) showed success in removing much <br />of flit flow impairment at or nr~ the production in[akt, <br />but the dilution lint was found pluggd and the 3Yr- to <br />2-I/16-in. annulus wu rtytrincd. Phase II was tcrmi- <br />rutd to considu alternative mrthtrdt far inaeuing the <br />ttrnpaarurc,t thc~ttom of the cavity. <br />PSsatt 111 of the cream injection rrsovery paiad atarttd <br />on July 6, 1971, with injmion of sttyrrt down the produc- <br />tarn robing in an atxmpt to inatasc tht oat production <br />tax by eking the trmpc-•a;yrc of the process volume at <br />tLc but A1d10ugh two backflow tyeles was a,ried out, <br />atom was coon injcntd continuously and in an upwud <br />direction. On July 12, 71 bbl of oil ^r niu nn~int from 0 <br />to 30 patent were tnekved through the l+c.atcr-treater. <br />'fhu oil was darks, o(lowa gnvity Ulan pRvitws pro- <br />duction. coouinra bitumen, and was ti~hdy emulsifid. <br />Oil pmduclinn decreased rapidly (to 5 B/D on July IB) <br />while incrrising in biwmcn wnrent. Biwmen upeet the <br />controls in tf,c surface facilities and sated misroul)ngs <br />of the diluent. lu solid content and rrsulunt density <br />Causrd name o(Iht heavy oils to be (lowed with tht water <br />to the disposal pit. Thar, solids wpold settle o: Inch out, <br />and the oil and biwmcn would float. From July 1B, <br />evidttfct inertued of plugting in the 2>'i-tn. tubing and <br />of cream bypass u,g Somc evidence of bypusing from <br />Ux. 7-in using to dst top of the cavity was availablt <br />almoi; from the ttan of -nut 111. Phue Ili wu termi• <br />oared on Aug. 3 for reuons of operating control: to <br />relieve stresses that the c~pansion of the wellhesd had <br />placed on the 355- and 2-1/I (r m. tubings and to wtss(der <br />how to proceed in the prcence of concentrations of Hr5 <br />that had ,nrreucd to the acttptable limits or the well <br />deign. <br />Aftc modi(icat;on to ttic wdlhtads for H,S compati• <br />biliq• and iRrsi relic( of tubings, Phut IV of tht stem <br />injection-rernvery period wu started on On. 19, 1971. ]t <br />was ttrminactd a: lY_c. 14, 1971, after (low impairment <br />occurred in the process volume and it had Ixcn estab- <br />lished that there w>.s unasoidable communication sad <br /> I u.r. l Mti! f l I ...,a n, wt.sst mi i w,av s i <br /> F ~ v = <br /> ~ :- <br /> o EE ~ c ~~ <br />~ ~ E <br /> c ~ t a ~ ! a <br />c <br />~ ~. <br /> a 'e ~ l <br />l <br />c 'v ax <br /> ~ ~ <br />~~~ •~ E <br /> z ~ ~ ~~ y$ ~ ~ <br />i $z: ~s o <br /> ~ : <br />i <br />~ <br />l ~ ~ a <br /> c _ is is IA _ ce <br />~j <br />~ r $R <br /> y t <br />.. - t <br />A I , ~ i <br />^al <br />i f <br /> <br /> <br />r <br />^ <br /> r- r „ M• YFa /~ r.r ar,t /-, aai M OC b~ MC <br />,a,l <br />R9 17-Summary d oper^toru- a~srape u+cy WnpararJ~ r• tm.. <br />tOee 1(X7RN~1. pF P1:.1Rt)L~ZJM 7ECN.VOI OGt' <br />r <br />
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