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HYDRO27153
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HYDRO27153
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Entry Properties
Last modified
8/24/2016 8:46:32 PM
Creation date
11/20/2007 7:37:11 PM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1999002
IBM Index Class Name
Hydrology
Doc Date
3/22/2004
Doc Name
Well 21-16 (CO3858-04565
From
American Soda L.L.P.
To
EPA
Media Type
D
Archive
No
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r <br />r~; <br />M~ ~9- ooh <br />zS ~ <br />AMERICAN/ Ed Cooley <br />S O D A, L L P Environmental Health and <br />Sofety Manager <br />2717 County flood 215 <br />Parachute. CO 81635 <br />Thursday, March ]8, 2004 <br />Elisabeth Evans <br />Director Technology Enforcement Program <br />U.S. Environmental Protection Agency / <br />Region VIII <br />999 18TM' Street, Suite 300 <br />Mail Code 8ENF-T <br />Denver, Colorado 80202-2466 <br />Re <br />Dear Elisabeth: <br />Direct Line {970) 285-0407 <br />International Telephone +l (970) 285-6500 <br />General Facsimile (970) 285-6393 <br />ENV.61.04 <br /> <br />MAR 2 2 2004 <br />Division of Minerals and Geology <br />Well 21-16 (C03858-04565) <br />In accordance with Minor modification b to EPA Area Permit No. C03858-00000 American <br />Soda LLP has made verbal notification and by copy of this letter is providing written <br />notification that Well 2l -16 (C03858-04565) had a sudden decrease in production return and <br />a drop in injection and production pressure. As soon as the operations personnel discovered <br />this change the following steps where initiated: <br />1. The well pressure, temperature and flow meters were checked for accuracy. <br />2. The well valves were checked for leakage. <br />When steps one and fwo did not correct the problem the following steps were initiated: <br />3. Injection into the well was discontinued. <br />4. A mechanical integrity test has been completed on the well casing and well tubing. <br />Both the casing and tubing demonstrate integrity. <br />5. A temperature log has been performed and there is no indication of upward <br />movement of fluids (copy attached), <br />Well 21-76 will be de-pressurized and maintained in a standby mode until a final <br />determination can be made to either request permission to re-inject into this well or to <br />Delivering a Crystal Clear Advantage <br />www.americansoda.com <br />
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