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HYDRO26589
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HYDRO26589
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Last modified
8/24/2016 8:46:03 PM
Creation date
11/20/2007 6:52:15 PM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1983194
IBM Index Class Name
Hydrology
Doc Date
10/14/2004
Doc Name
BLM Sundry Notices for Plugging and Abandonment and EPA Plugging Record for Injection Wells
From
Natural Soda Inc.
To
DMG
Media Type
D
Archive
No
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lA-4HI WELL <br />PLUG AND ABANDONMENT <br />8/16/2004 <br />Rig up rig on well. Remove longer section of flow line from work area. Heat up well <br />head with weed burners. Pull up to 45K with sling chokers on 5-1/2 casing. Parted <br />chokers. Shut down and await casing crew. <br />8/17/2004 <br />T&N casing crew on location. Put 5-1/2 elevators on casing and bails. Pulled to 80K. <br />Heated and beat well head. Pulled 80K plus. Cut 7 inch casing below well head. Well <br />head dropped. Cut''/z inch notch out of 7-inch casing. Well head dropped. 5-/2 inch <br />casing in tension. Picked up 5-1/2 casing cutter and 2-7/8 tubing. Run in well to 1175 feet <br />and tagged solid. Pull back out of well. Run in well with 4-3/4 inch bit. Rig up tank and <br />pump. Run bit in well. Tagged solid at 2240 feet. Pulled out of well. Ran cutter to 2010 <br />feet, M.D. (1900 TVD) Shut down for night. <br />8/18/2004 <br />Run cutter rest of the way in well to 2220 ft. MD, (1945 ft. TVD). Cut casing. Pull out of <br />well with tubing and cutter. Tried pulling casing. Would not come out. Started running <br />cutter into well to make higher cut. Casing parted. Pulled tubing and casing cutter back <br />out of well. Pulled casing 10 feet out of well and shut down to await casing crew and <br />water truck. Flushed casing with hot water. Pulled 5-1/2 inch casing from well. Pulled 52 <br />and''/z joints of casing out of well. Left 2 and `/~ joints in well. Shut down for night. <br />8/19/2004 <br />Run 6-1/8 inch bit and scraper in well. Tag at 2215 feet. Run 7-inch Cast iron bridge plug <br />( CIBP) in well and set at 2210 feet. Pulled running tools out of well and ran tubing back <br />into well open ended to 2200 for pumping cement. Shut down for day. <br />8/20/2004 <br />Rig on stand-by. Awaiting cement trucks. <br />8/23/2004 <br />Rig up Big 4 cement trucks to well. Pump 40 sacks 15.8# cement with 3% calcium <br />chloride into well. Pull out of we11300 feet with tubing. Wait 2 hours on cement. Run in <br />well and tag cement at 1940 +/- feet. Pump 250 sacks of 12.4# cement with additives to <br />surface. Pull tubing from well, laying down on trailer. Rig down. <br />24 September 2004 <br />Grout well to surface. Install dry hole marker. <br />
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