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HYDRO20112
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HYDRO20112
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Last modified
8/24/2016 8:41:30 PM
Creation date
11/20/2007 1:22:01 PM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
C1989074
IBM Index Class Name
Hydrology
Doc Date
5/12/1998
Doc Name
SEDIMENT POND CERTIFICATION AT RIMROCK MINE
From
GREG LEWICKI & ASSOCIATES
To
MLRD
Permit Index Doc Type
SEDIMENT POND INSPECTIONS
Media Type
D
Archive
No
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<br />' Rimrock Mine Sediment Pond Certification <br />The site inspection was conducted on May 9, 1998. It wa a clear day of 65 degree <br />temperature and it had not rained in the previous few da s. The pond contained <br />.approximately 1.5 feet of clear water, which was wey elow the principal spillway <br />pipe. Engleville Gulch was flowing approximately 0.8-1.2 gallons per minute. The <br />pond is to be left as a permanent impoundment for use in the grazing operation. <br />The following items were checked to see if they coincided with the design shown in <br />the mine permit application. I, Gieg Lewicki, did the pond design in March of 1990. <br />1) Constructed Elevations: The elevations listed below were checked with a precision <br />level and stadia rod: <br />-Dewatering pipe inlet <br />-Dewatering pipe outlet <br />-Top of Dam <br />-Bottom of Emergency Spillway <br />-Toe of Dam (outside and inside) <br />-Bottom of Pond <br />-A number of points within the pond <br />All elevations were found to be acceptable. The inlet to the principal spillway was <br />placed at a slightly higher elevation to allow more sediment storage. The 10 year - 24 <br />hour runoff storage was still present above the principal spillway. <br />2) Width of Emergency Spillway Design: 12 feet. Measured: 12.2 feet. <br />3) Depth of Emergency Spillway Design: 1.55 feet. Measured: 1.60 feet. The spillway <br />showed nb evidence of flow or any signs of erosion or other instability. <br />4) Width of top of Dam Design: 10 ft. Measured: 10.2 ft - 10.6 feet. <br />5) Principal S iIR~X Design: 4.0" pipe placed in compacted embankment. Measured: <br />4" steel pipe placed in compacted embankment. Extensions on this pipe were added to <br />both sides so that the embankment could be widened. Some black, plastic hose was also <br />present near the spillway at the time of the inspection but was not functional. The <br />principal spil]way pipe was completely free of debris and was functional during the <br />site visit. <br /> <br />
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