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(Page 3) <br />MINE ID # OR PROSPECTING ID # M-1999-002 <br />INSPECTION DATE 21/08/04 <br />INSPECTOR'S INITIALS ESC <br />• Well 21-16; Well pernanently abandoned and the well head has been cut off below <br />the surface. The piping and skids will be removed and the pads and roads will be <br />graded and seeded this fall or next spring. The entrance road to 21-16, 28-17 and <br />28-41 will remain as a storage laydown area. <br />• Well 28-17; Well permanently abandoned and the well head has been cut off below <br />the surface. The piping and skids will be removed and the pads and roads will be <br />graded and seeded this fall or next spring. <br />• Well 28-41; Well permanently abandoned and the well head has been cut off below <br />the surface. The piping and skids will be removed and the pads and roads will be <br />graded and seeded this fall or next spring. <br />• Well 29-51; Well permanently abandoned (only drilled to 250 feet) and the well <br />head has been cut off below the surface. The mud pits have been graded. <br />• Well 20-6; Well was plugged and capped back in 2000. Pad area will be graded and <br />seeded. The road will be graded and the drainage area will be reshaped. <br />• Well 20-32; American Soda intended for this well to be placed in Long Term <br />Standby. Problems occurred to the well when the casing was pulled and would not <br />hold the required pressure. Therefore, the well was permanently abandoned. Road <br />will remain to access future drill pads. <br />• well 20-35; American Soda intended for this well to be placed in Long Term <br />Standby. Problems occurred to the well when the casing was pulled and would not <br />hold the required pressure. The well has been permanently abandoned. <br />• Well 20-31; American Soda intended for this well to be placed in Long Term <br />Standby. Problems occurred to the well when the casing was pulled and would not <br />hold the required pressure. The well has been permanently abandoned. <br />• Well 20-30; Well plugged. One casing was producing gas. This well will undergo <br />a pressure test to determine if the temporary seal is adequate. <br />• Well 20-76; American Soda intended for this well to be placed in Long Term <br />Standby. Problems occurred to the well when the casing was pulled and would not <br />hold the required pressure. The well has been permanently abandoned. <br />• Well 29-68; American Soda intended for this well to be placed in Long Term <br />standby. Problems occurred to the well when the casing was pulled and would not <br />hold the required pressure. The well has been permanently abandoned. <br />• Well 29-23; Well placed in Long Term Standby. The skid has been stored adjacent <br />to the well. <br />• Well 29-53; American Soda intended for this well to be placed in Long Term <br />Standby. Problems occurred to the well when the casing was pulled and would not <br />hold the required pressure. The well has been permanently abandoned. <br />• Well 29-24; Well placed in Long Term Standby. Nacholite residue will need to be <br />cleaned up from the pad area. <br />• Well 28-21; Well placed in Long Term Standby. The skid has been stored adjacent <br />to the well. <br />2 & 8 Contact Address <br /> ^ CE <br />NAME Mr. Ed Cooley ^ BL <br />OPERATOR American Soda, L.L.P. fl FS <br />STREET 2717 CR 215 ^ HW <br />CITY/STATE/ZIP Parachute, CO 81635 ^ HMWMD (CH) <br /> ^ SE <br /> ^ WQCD (CH) <br />Cc: Carl Mount; DMG <br />