Laserfiche WebLink
DAM NAME: San Luis Tailing Dam DATE OF REPORT: 06 20 18 <br /> TAILING DAM INSPECTION FORM <br /> Directions: Mark an ✓for conditions found and underline words that apply <br /> SEEPAGE AND DRAIN OUTFALL <br /> PROBLEMS NOTED: ❑(30)NONE ❑(31)SATURATED EMBANKMENT AREA ❑(32)SEEPAGE EXITS ON DAM <br /> ❑(33)SEEPAGE EXITS AT POINT SOURCE 0(34)MINOR PONDING OF PIPE LEAKAGE AT TOE <br /> DRAIN OUTFALL SEEN: 0 YES ❑NO ❑(35)FLOW ADJACENT TO DRAIN PIPE ❑(36)DRAIN OUTFLOW TURBID <br /> ❑(37)DRAIN DRY/OBSTRUCTED 0(38)OTHER: See comment. <br /> SHOW LOCATION OF DRAIN ON SKETCH <br /> AND INDICATE AMOUNT AND QUALITY OF SEEPAGE <br /> See Figure 1 for location. Photos 13-16:Toe drain manifold collection pipe was disconnected at time of inspection. <br /> All 3 pipes appeared to be flowing clear. Seepage quantity not estimated due to partially submerged exit conditions. <br /> Storm-water runoff sediment accumulation from right groin area continues to be a minor maintenance/access issue <br /> in the toe area. <br /> CONDITIONS OBSERVED: Z GOOD ❑ACCEPTABLE ❑POOR <br /> STORM WATER MANAGEMENT SYSTEM <br /> PROBLEMS NOTED: ❑(40)NONE ❑(41)NO EMERGENCY SPILLWAY <br /> ❑(42)EROSION AT DROP STRUCTURE ❑(43)CONCRETE DETERIORATED/UNDERMINED ❑(45)STRUCTURE MAY BE TOO SMALL <br /> ❑(46)DIVERSION CHANNEL EROSION ❑(47)INADEQUATE CHANNEL FLOW CAPACITY ❑(48)CHANNEL FLOW OBSTRUCTED <br /> 0(49)OTHER: Photos 9-11: South Diversion Ditch drop structure replacement project was under construction at <br /> the time of inspection. During construction, storm water from upstream watershed is being contained in the channel <br /> by a cofferdam (berm) constructed across the ditch channel upstream from the structure. <br /> CONDITIONS OBSERVED: ❑GOOD ❑ACCEPTABLE ❑POOR <br /> MONITORING <br /> EXISTING INSTRUMENTATION FOUND: ❑(50)NONE ❑(51)GAGE ROD IN POOL AREA 0(52)PIEZOMETERS <br /> ❑(53)SEEPAGE WEIRS/FLUMES ❑(54)SURVEY MONUMENTS 0(55)OTHER: Underseepage flows <br /> MONITORING OF INSTRUMENTATION: ❑(56)NO 0(57)YES <br /> PERIODIC INSPECTIONS BY: 0(58)OWNER ❑(59)ENGINEER <br /> See attached piezometer measurements-all instruments remain dry; underseepage flow rates (measured at outfall <br /> pipe) remain steady at approximately 40 gpm. <br /> CONDITIONS OBSERVED: 0 GOOD ❑ACCEPTABLE ❑POOR <br /> MAINTENANCE AND REPAIRS <br /> PROBLEMS NOTED: ❑(60)NONE ❑(61)ACCESS ROAD NEEDS MAINTENANCE ❑(62)CATTLE DAMAGE <br /> ❑(63)BRUSH ON: UPSTREAM SLOPE/BEACH,CREST,DOWNSTREAM SLOPE,TOE <br /> ❑(64)RODENT ACTIVITY ON: UPSTREAM SLOPE/BEACH,CREST,DOWNSTREAM SLOPE,TOE <br /> 0(65)OTHER: Continue to maintain surface erosion controls(cross berms and rock-lined downspouts)in right d/s groin repair area,and <br /> repair minor gullying in upper left abutment groin near access road where runoff is bypassing the lined ditch. Consider re-directing surface <br /> runoff from right lower groin away from d/s toe area to prevent deposition of sediment. <br /> CONDITIONS OBSERVED: 0 GOOD ❑ACCEPTABLE ❑POOR <br /> OVERALL CONDITIONS <br /> Based on this inspection and recent file review,the overall surficial condition is determined to be: <br /> 0 SATISFACTORY ❑CONDITIONALLY SATISFACTORY ❑UNSATISFACTORY <br /> Page 2 of 4 <br />