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r <br />Transit Mix Concrete Co. <br />BRIERLEY <br />ASSOCIATES DAILY FIELD REPORT <br />Project <br />Daniel Sand W3sIt Fine Pit <br />Location <br />Colorado Springs. CO <br />Client <br />Tram -it 11fix <br />Contractor <br />Pioneer Sand Civil Canstntcrioti <br />Meather <br />Sonny <br />I. CONTRACTOR'S ACTI4'=S; <br />Report 1o_ <br />OO.t <br />Date <br />5.1,16-2017 <br />Page <br />3 <br />100 <br />File No. <br />516051400 <br />Temperature <br />43-722F <br />Pioacer crew consisted of 6 laborers imludiq foreman Robert )antes_ Two of the Iaborers were from <br />Mauls Coustructtoa. <br />At 0705 lus_ dozer beton worLtug on ley excavation near �taliou 1+00 Two sm. pen began excavatinit <br />within pond footprint and transporting soil to the new route/haul road. <br />At 0715 hrs. n%v additional scrapers began excavating within pond footprint and tnuisportkit soil to die <br />new rotuelaid road. <br />At 0720 lus_ walked key excavation centerline from station l ' 00 to 8.00 to inspect progress. Bear ctarnon <br />I+00 and 2+00, nater pondi*exposed in coarse sand layer. Water pondcd within bottow of key hear <br />station 4+00 and 4+50. key width is approximately 15 feet <br />At 0745 firs. Robert (Pioneer) and Grant (Trausit NUx) shot key depth at station 1-50 and 2+50 Elevation <br />was shallow at both locations. However due to the presencc of u7ilcr near station 1-50. key excavation did <br />not go deeper. <br />At 0800 his. scraper rent ved approximately one foot of sod from kcy at station 2+50 io reach ley depth of <br />10 feet, <br />At 0810 lirs, scarified with dozer key excavation from station 1+00 to 4+00 <br />At 0815 hrs, dozer created access road for scraper near station 4+00 to allow for compaction of subgrade <br />At 0820 firs. scraper smoothing the eastern toe of dant from station 1 00 to 4+00 <br />At 0830 firs. scarified with dozer key excavation from station 6+00 to 8+00. <br />At 0845 firs. moisture conditioning Ley with water tarok frow station 6+00 to 8+00. <br />At 08501trs. dozer compsictin?Acveling key from station 6+00 to 5+00 <br />At 0900lus. doze vv'uikiitg uu iicvv routellrvt,l road Filling up v.1ter tank. <br />Ar 0930 tis. Eutech (Stu and )ill) onsite to perforin nuclear density tests on the key lifts. Entecli sad <br />samplc had a tuaxurmut dry density of 124 pcf and optimum woistine content of 10 percent. <br />At 0945 Ius, moisture condrtiotang key 111111 water lank front station 6+00 to B+00. <br />At 1000 his. Entech using unclear density gatige at two locarions along souther kc)' subgrnde. Tests <br />indicated 90 percent relative compaction and motsnire couteut 8-11 ptrcetu. <br />At I020 hrs, scraper with full can of sol! performed several passes eloug key from station 6+00 to 8+00 in <br />order to couipact the stibgrnde <br />Rage I cf 3 <br />