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2016-10-21_REPORT - M1980244 (31)
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2016-10-21_REPORT - M1980244 (31)
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Entry Properties
Last modified
1/9/2017 10:52:55 AM
Creation date
12/22/2016 8:15:33 AM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1980244
IBM Index Class Name
Report
Doc Date
10/21/2016
Doc Name
SGVLF Phase I Cert Report - 0 Completion Report
From
CC&V
To
DRMS
Type & Sequence
TR87
Email Name
TC1
AME
ERR
Media Type
D
Archive
No
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Cripple Creek & Victor Gold Mining Company <br />Squaw Gulch VLF Phase 1 Completion <br />Record of Construction Report <br />475.0106.006 <br />October 14, 2016 <br /> <br />P:\Projects\0106.006 CC&V CQA and EDS\J‐REPORTS\ROC Report\475.0106.006 CCV PHASE 1 ROC REPORT ‐ FINAL161014.DOCX <br /> Page 6 <br />2.7. Soil Liner Fill <br />Approximately 101,690 cy of SLF was placed within the Squaw Gulch VLF Phase 1 Completion <br />area. The as‐built SLF surface is presented in Record Drawing No. 2. <br />Materials from the Cameron borrow and WHEX pit were processed through a custom‐designed <br />rotary mill and screen in order to remove oversized rock and uniformly condition the material. <br />After processing, the SLF was stockpiled in designated stockpiles around the site. <br />Ames used CAT 740 articulated haul trucks to haul SLF from the local stockpiles to the Squaw <br />Gulch VLF Phase 1 footprint. The material was spread using CAT LGP dozers equipped with GPS, <br />and moisture conditioned in place by tandem‐axel water trucks and laborers. CAT 10‐ton <br />smooth drum vibratory compactors and vibratory plate compactors were utilized to compact <br />the SLF to a minimum thickness of 12 inches. The specified minimum density was 95 percent of <br />the maximum dry density at minus 2 percent to plus 3 percent of optimum moisture content as <br />determined by ASTM D698. <br />Laboratory testing, moisture content verification, nuclear density testing, depth verification, <br />and visual inspection of the SLF were performed by the CQA Monitor prior to approval for <br />geomembrane deployment. If deficient areas of the SLF were encountered, the area was <br />reworked and retested until the area was compliant with the project technical specifications. <br />All SLF was inspected and approved by the CQA Monitor, CC&V, Ames and ECA prior to <br />geomembrane deployment. SLF acceptance is discussed further in Section 3.2.5 and Section <br />3.4.2. SLF acceptance forms are provided in Appendix E. <br />2.8. Geomembrane <br />ECA installed approximately 2,729,600 square feet of 80 mil LLDPE DSMS geomembrane within <br />the Squaw Gulch VLF Phase 1 Completion area as shown on Record Drawing No. 6. Due to an <br />insufficient inventory of 80 mil LLDPE DSMS geomembrane, the last thirteen panels (P‐2486 <br />through P‐2498) of geomembrane that were installed consisted of 100 mil single sided textured <br />(approximately 7,000 square feet) and 100 mil smooth (approximately 9,000 square feet) LLDPE <br />geomembrane. The 100 mil LLDPE geomembrane was the excess material that had been <br />approved for use within the Pregnant Solution Storage Area (PSSA). The use of 100 mill <br />geomembrane is discussed further in Section 4 of this report. <br />Fork lifts were used to transport and deploy the geomembrane panels parallel to the slopes to <br />minimize stress on seams. Double‐wedge fusion welding was the primary method of <br />geomembrane seaming. Extrusion welding methods were used to perform tie‐in seaming, <br />defect repairs, and detail activities. Continuity conformance of fusion welded seams was <br />performed using pressure testing methods, while extrusion welded seams and repairs were
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