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2016-08-01_REPORT - M1980244
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2016-08-01_REPORT - M1980244
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Entry Properties
Last modified
12/4/2020 3:49:05 AM
Creation date
8/1/2016 2:47:28 PM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
M1980244
IBM Index Class Name
Report
Doc Date
8/1/2016
Doc Name
Weekly Construction Quality
From
Newmont
To
DRMS
Email Name
TC1
Media Type
D
Archive
No
Tags
DRMS Re-OCR
Description:
Signifies Re-OCR Process Performed
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Newmont Mining Corporation Boo <br /> Cripple Creek&Victor Gold Mine . <br /> Squaw Gulch VLF CCLA <br /> NewFields Job No.475.0106.006 <br /> Week Ending Saturday,July 23,2016 <br /> using three fusion welding machine/operator combinations. Eighteen destructive testing <br /> samples were marked during fusion seaming. Approximately 770 linear feet of seam was <br /> extrusion welded using one extrusion welding machine/operator combination. Four destructive <br /> testing samples were marked during extrusion seaming. All destructive tests performed met <br /> project specifications. Non-destructive testing was performed for fusion welded seams. Repairs <br /> were performed using the extrusion welding method for all marked defects. Vacuum testing <br /> was performed for all extrusion welded seams and repairs. <br /> 2.3 Anchor Trench <br /> Approximately 500 feet of interim anchor trench was excavated along the Phase 1 9,950-foot <br /> bench and 625 feet of permanent anchor trench was excavated along the Phase 1 perimeter <br /> between the 9,850-foot and 9,950-foot bench in accordance with design drawings and project <br /> technical specifications. <br /> Anchor trench backfill was performed using a skid steer, a vibratory plate compactor and <br /> laborers. A NewFields representative monitored the backfill procedures to ensure that the <br /> anchor trench was constructed in accordance with the design drawings and project technical <br /> specifications. <br /> 2.4 Geomembrane Acceptance <br /> Panels P-2008 through P-2025 and P-2027 through P-2066 were accepted for Drain Cover Fill <br /> placement. The attached Figure 3 shows the acceptance areas. <br /> 3.0 STORM WATER MANAGEMENT <br /> Best Management Practices continued to be performed. <br /> 4.0 NEWFIELDS LABORATORY ACTIVITIES <br /> NewFields personnel performed sieve analysis, atterberg limits, compaction and permeability <br /> testing. The following samples were collected for laboratory testing: <br /> Soil Liner Fill: NFSLF-39-C and NFSLF-41-C (Dump 1 Processing Plant) <br /> Soil Liner Fill: NFSLF-40-R (Phase 1 VLF) <br /> Drain Cover Fill: NFDCF-9-R (Phase 1 VLF) <br /> Page 4 <br />
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