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overflow lip is at elevation 5555.0. There is a pair of 6 -inch diameter valves in the riser with <br />invert at elevation 5552.0, which sets the maximum normal pool at this level. The pond is <br />normally operated as a "pass through" design with both valves left in the open condition. In <br />addition, there are three parallel 18 -inch diameter 20 -foot long horizontal corrugated metal pipes <br />with upstream invert elevation 5557.0 which serve as an emergency spillway system. <br />Inflow Calculation Results <br />The results of the runoff calculations and synthesized constant inflow are presented in the <br />attached SEDCAD model printouts. The system was modeled using SEDCAD for its response to <br />a 10 year, 24 hour storm of 2.0 inches for the sediment control analysis, and the 25 year, 24 hour <br />storm of 2.4 inches for the spillway evaluation. In both cases, a constant base case inflow of <br />1,000 gpm was also included. For continuity, the results of these models are presented below <br />along with the discussion of the physical dimensions and properties of the pond. <br />The volume of the below grade pond was input into the SEDCAD model, along with its spillway <br />details. The model watersheds were input as a series of sub -watersheds, each with its own <br />acreage, its own flow response parameters (slope, distance, time of concentration), and the <br />specific runoff Curve Numbers from Table 2.05.3(3)-lA. The 10 year, 24 hour storm was then <br />applied to the composite watershed, and routed down to the sediment pond. SEDCAD allows <br />the user to override the customary starting pool that is set by the lowest drain hole. In the case of <br />the 10 year storm, where the starting pool is normally set by the twin 6 -inch valves with invert at <br />elevation 5552.0, the starting pool at the start of the design storm needs to be 1.43 feet higher, or <br />elevation 5553.43 to account for the 1,000 gpm already flowing through the two orifices at the <br />start of the storm. It can be observed in the SEDCAD printout that the storm and fixed inflow <br />generate runoff of 6.12 ac ft of inflow and that the pool rises to 5554.32 feet during the routing <br />of this event. The SEDCAD results show the pond has a trap efficiency of 66.8°/x, and it releases <br />water with a 24-hour weighted settleable solids concentration of 0.11 ml/1, well below the 0.50 <br />ml/1 standard. <br />The 25 year, 24 hour storm has also been modeled as the spillway design event. For this <br />analysis, it has been conservatively assumed that the twin 6 -inch orifice holes are closed, and <br />normal starting pool is the principal spillway elevation of 5555.0. This must be raised 0.23 feet <br />to account for the 1,000 gpm over the riser lip, treated as a sharp -crested weir. The starting pool <br />for the 25 year spillway design storm was thus set to elevation 5555.23. The runoff combined <br />with the constant inflow produce a total runoff volume of 9.14 ac -ft. In the attached SEDCAD <br />printout for that storm it can be observed that the pool only rises to elevation. 5556.10, or 1.10 <br />feet above the riser pipe overflow. As such, the routed 25 year storm does not raise the pool high <br />enough to engage the three horizontal CMPs at El 5557.0, which are the emergency spillway. <br />The following table summarizes the storm response flow. <br />Pond 013 SEDCAD Results - With Fixed Inflow <br />Attachment 2.05.3(3)-32 Revision Date: 3/09/2016 <br />Page 4 Revision No.: TR -70 <br />SEDCAD <br />Peak <br />Case <br />Q;,,, cfs <br />Pool, ft <br />SS mUl out <br />10 yr, 24 hr sedimentation storm 34.19 <br />5554.32 0.11 <br />25 yr, 24 hr spillway design storm 48.06 <br />5556.10 n/a <br />Attachment 2.05.3(3)-32 Revision Date: 3/09/2016 <br />Page 4 Revision No.: TR -70 <br />