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BRIERLEY DAILY FIELD REPORT <br /> ASSOCIATES <br /> Creating ipoce Unew9couno <br /> ' Project Hokestra-North Slurry Wall Report No. 6 <br /> Location Firestone, CO Date Wednesday, May 01, 2013 <br /> Client Hall-Irwin Page 2 of 4 <br /> Contractor Hall-Irwin File No. 112206-000 <br /> Weather Windy with Snow Showers Temperature Very Cold(0°-32°) <br /> Quality Location or Batch Results Comments <br /> ' Control 7T <br /> Soil-Bentonite Backfill <br /> Unit Weight 8+10, 8+85 119.6, 120.4 pcf <br /> ' Slump 8+10, 8+85 6.00, 4.75 inches <br /> -200 Wash 8+10 5 1.1% passing No. 200 <br /> t Triaxial <br /> Permeability Next sample to be taken at station <br /> 15+00 <br /> Test <br /> Cement Stabilized Soil-Bentonite Backfill(when applicable) <br /> Unit Weight XX pcf N/A <br /> Slump XX inches N/A <br /> Gradation XX% passing No. 200 N/A <br /> Verified Depth <br /> Verified ® Yes <br /> Clean AM ❑ No <br /> Backfill <br /> Slope and <br /> ' Bottom of <br /> Key <br /> ® Yes 8+85--*9+20,9+20—>9+55, <br /> Verified ❑ No 9+55--+9+90,9+90-->10+25, 4ft key(23 ft total depth),4ft key <br /> Depth To 10+25--*10+60 (23 ft total depth),4ft key(21 ft <br /> Bedrock and total depth),4ft key(21 ft total <br /> Key depth),4ft key(23ft total depth) <br /> Bedrock Samples Top: 8:30 AM, 10:00 AM, 11:30 <br /> Frequency = Once per 100LF of 9+90 AM,2:33 PM,3:57 PM <br /> slurry wall Bottom:9:15 AM, 11:00 AM, <br /> ' 12:30PM,3:OOPM,4:45 PM <br /> Average Excavation Time of Bedrock 0.80 Hrs <br /> per Set <br /> III. NOTES: <br /> ' 1. Hall-Irwin(HI)on-site using a Komatsu PC 800 Excavator to remove alluvium material from the slurry <br /> trench. Fresh slurry was placed within trench as work progressed up-station to keep the walls of the <br /> trench from collapsing. Backfill material was mixed and placed throughout the day. <br />