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2015-05-18_REVISION - C1980007 (2)
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2015-05-18_REVISION - C1980007 (2)
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Entry Properties
Last modified
8/24/2016 6:00:26 PM
Creation date
5/18/2015 1:25:24 PM
Metadata
Fields
Template:
DRMS Permit Index
Permit No
C1980007
IBM Index Class Name
Revision
Doc Date
5/18/2015
Doc Name
Letter & Application (Emailed)
From
Mountain Coal Company
To
DRMS
Type & Sequence
SL8
Email Name
JRS
MPB
Media Type
D
Archive
No
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Boatt Longypar Drilling Services <br />2745 California Avenue Salt Lake City, Utah 84104 -4579 <br />WELL ABANDONMENT REPORT <br />Date: 912014 <br />Well Identification <br />Owner Mountain Coal Company <br />Well Number E3 -32.5 <br />Well Location (township & range) T13S, R90W <br />(Lat/Long) 38' 52' 30.1" 107 26' 17.2" <br />_) <br />County Gunnison State co <br />Elevation 7772' <br />Existing Well Details <br />Is the well drillers report provided? Yes X No <br />Nature of use & current status Degas Well /capped <br />_ _ <br />Role Depth 700 Feet Hole Diameter <br />12.25/8.75 Inches <br />Surface Casing Type /Wt. J -55 Steel / 65# Size <br />19" Depth 20' <br />Intennediate Casing Type /Wt. J -55 Steel / 32# Size <br />9.625 "Depth 625' <br />Completion Blank Casing Type /Wt. J -55 Steel / 174 <br />Size 7" Depth 577 -619' <br />Completion Perf Casing Type /Wt. -55 Steel�1 17# Size _T' Depth 619 -700'_ <br />_J <br />Static Fluid Level depth N/A Feet Artesian Flow <br />—N/A GPM <br />Shut -in Pressure N/A PSI <br />Notes <br />Abandonment Details <br />Reason for Abandonment No longer needed <br />Bridge Plug Type Dubber Ton -Job cementing- plu� <br />TD of well or Bridge Plug Depth 141 Feet <br />Total fluid volume of well from TD or Bridge Plug 284 Gallons <br />Sealing Material Used _Hole Plug. Portland Cement <br />Method of sealing material placement _Pumped hole plug and cement from surface <br />Casing cut to _5— Ft. below the surface P & A Marker type Aluminum cap with rebar pin <br />Date of Abandonment Completion 9/2014 <br />Notes To -Job Plu st2pred at 78' and could not be forced down agy further <br />* All depths are from top of surface casing <br />
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