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2014. One well string, 29-26 short string, failed the MIT test and will be scheduled for plugging <br /> and abandoned in the third quarter 2014. <br /> L <br /> F,- <br /> p ' <br /> Photo 3 — Mechanical Integrity Testing (MIT) equipment connected and operating while pressure test is in <br /> progress on solution mining well in early June 2014. Wells are pressured to approximately 400 PSI for 30 minutes <br /> during the testing. The short string on production well 29-26 failed to hold pressure and will be plugged and <br /> abandoned using tremie line cement placement through shallow coil in the third quarter of 2014. <br /> When the short string of well 28-21 was plugged and abandoned in 2012 no production well <br /> strings remained open on the lateral leg accessing this production well pad. During the early <br /> summer of 2013 all of the lateral piping, well skids and ancillary structures were removed from <br /> the complete lateral leg beginning at the main well field road intersection to this lateral. Two <br /> sections of the lateral piping that extended through the established trees were removed <br /> without disturbing the vegetation. All other pipelines followed the path of the road. <br /> American Soda, L.L.P. 4 <br /> DRMS Annual Report <br /> July 10,2014 <br />