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BHA No. 1 was tripped out of the hole at 20:30 hours on August 27, 2013. The BHA No. 2 <br />was built up and run in the hole. BHA No. 2 was a directional drilling assembly which <br />consisted of, in part, a 9.875 -inch Reed type LHA517G tri -cone rock bit (Serial No. 07 -05- <br />21118) and a 6.75 -inch mud motor (Serial No. 6819) with a 2.5 degree bend EM (electro- <br />magnetic) transmission tool. A gamma detector was spaced 35.5 feet behind the bit to aid <br />in correlation while drilling to the intermediate casing point. The kick -off point (KOP) for <br />building the curve part of the hole was reported in the SDI End of Well (EOW) Report as <br />1,488 feet MD KB. <br />Capstar began drilling with BHA No. 2 at 1,444 feet MD KB at 01:30 hours on <br />August 28, 2013. The intermediate hole TD of 2,230 feet MD KB, was reached by 18:00 <br />hours on August 30th with full circulation. The hole was circulated and conditioned for one <br />hour prior to tripping out of the hole. At approximately 2,000 feet MD KB, the pipe pulled <br />tight and while working it free the draw works drive chain broke. Repairs were made <br />quickly (1.5 hours) and the pipe was worked free. BHA No. 2 was tripped out of the hole <br />and laid down. The reaming assembly was picked up and run back in the hole after the <br />drilling line was slipped and cut. <br />The reaming assembly was tripped in to 1,444 feet MD KB where it tagged up, and was <br />washed and reamed the rest of the way to bottom at 2,230 feet MD KB with full <br />circulation. The reaming assembly was tripped out of the hole. Fifty joints of 7.625 -inch <br />26.4 ppf K -55 casing was run in the hole. The shoe was landed at 2,229 feet MD KB on <br />August 31, 2013 at 23:30 hours. The connections on the first three joints were tack - <br />welded and the casing was circulated every 5 joints after reaching 1,400 feet MD KB. The <br />casing was circulated on bottom and an LCM sweep was pumped with full circulation. <br />The Halliburton cementing crew was rigged up at 02:30 hours on September 1, 2013 after <br />participating in a pre -job safety meeting. The following cement mixture was mixed and <br />pumped: 10 bbls water, 20 bbls Superflush, 10 bbls water, 141 bbls (500 sacks) of 14 ppg <br />Daub & Associates, Inc. Page 3 of 7 13H -R Well Summary Report <br />