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<br />. <br /> <br />the pipe, Based on the video inspection, it appeared that the majority of the pipe was structurally sound, with the <br />exception of the east end where the intake structure is located, It appears that the upper portion of the outlet pipe, <br />immediately downstream of the intake structure had collapsed/failed, This pipe failure appears to be associated with <br />the slope failure/slide that occurred along the upstream face of the embankment <br /> <br />An area of apparent seepage was observed along the southern groin of the downstream face of the embankment in <br />the natural soils situated uphill of the outlet We have not observed any seepage or standing water in this area <br />during the last year, however the area is vegetated with wetland type grasses indicating a significant water source, <br />Based on our review of the State Engineer's records, it appears that seepage had been previously observed in this <br />area while the reservoir was holding water and the area was heavily vegetated with willows. It appears that the <br />willows have been removed sometime between the State Engineer's inspection in 1996 and our first site visit in <br />September of2000, <br /> <br />. <br /> <br />The spillway for the reservoir is situated approximately 125 feet southeast of the south end of the embankment The <br />spillway appears to have been excavated into the natural soils and was approximately 18 feet in width. However, <br />the client had constructed a stop log structure in the spillway, which reduces the effective width of the spillway to <br />approximately 8 feet The spillway flows to the south-southwest away from dam and then discharges into a natural <br />drainage way situated several hundred feet to the southwest of the dam. <br /> <br />Field Investigations <br /> <br />The field investigations for this project were conducted on October 10, 2000 and August 8, 2001. Five (5) test holes <br />were drilled at the approximate locations shown on Figure #2 to explore the subsurface conditions in the upstream <br />face of the embankment and in the proposed borrow area situated to the east of the existing spillway, A second field <br />investigation was conducted on August 8, 200 I to evaluate the proposed borrow area located at the east end of the <br />reservoir. Four test pits were excavated in this area and the approximate test pit locations are shown in Figure #2, <br />The locations of the test holes and test pits were determined by a representative ofNWCC, Inc, in the field and the <br />actual locations and elevations were determined by an instrument survey completed by Baker & Associates in <br />August of 200 1. <br /> <br />. <br /> <br />The test holes were advanced through the overburden soils and bedrock with an all-terrain CME 55 drill rig utilizing <br />4-inch diameter continuous flight power augers and the test pits were excavated with a Case CK backhoe, The test <br />holes and pits were logged in the field by an engineer from NWCC, Inc, <br /> <br />Samples of the subsurface materials were taken with a 2-inch 1.0, spoon sampler, The sampler was driven into the <br />various strata with a 140-pound hammer falling 30 inches, This test is similar to the standard penetration test <br />described by ASTM Method 0-1586. Penetration values, when properly evaluated, indicate the relative density or <br />consistency of the soils and bedrock, Large and small disturbed bulk samples were also obtained from the auger <br />cuttings and sides of the test pit excavations, Depths at which the samples were taken are shown on the Logs of the <br />Exploratory Test Holes and Test Pits in Figures #3 and #4. The Legend and Notes associated with the logs are <br />shown in Figures #5 and #6, respectively, Slotted, 2-inch diameter PVC casing was also installed in the three test <br />holes drilled in the embankment The temporary casings were installed so that the groundwater levels/phreatic <br />surfaces under the embankment could be monitored in the future and to try to determine the failure surface of the <br />failed soils, The bottom 15 feet of casing was slotted and the upper portion of the holes were cased with solid PVC. <br /> <br />. <br /> <br />Job Number: 00-4660 <br /> <br />NWCC, Ine, <br /> <br />Page 3 <br />