My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
PROJ00158
CWCB
>
Loan Projects
>
Backfile
>
1-1000
>
PROJ00158
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
4/18/2011 1:47:52 PM
Creation date
10/5/2006 11:41:04 PM
Metadata
Fields
Template:
Loan Projects
Contract/PO #
C150098
Contractor Name
Lake Henry Reservoir Company
Contract Type
Loan
Water District
17
County
Crowley
Bill Number
HB 02-1152
Loan Projects - Doc Type
Feasibility Study
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
79
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
Show annotations
View images
View plain text
<br />, <br /> <br />RECEIVED <br /> <br />June 9, 1995 <br /> <br />JUN 1 3'95 <br /> <br />INCIDENT REPORT <br /> <br />Lake Henry <br /> <br />WATER RESOl'RCES <br />STATE ENGIEER <br />QJI.O <br /> <br />w, Div, 2, DAMID: 170203 <br /> <br />At approximately 2:30 P,M., I was notified by Allen Ringle, Lake <br />Henry Reservoir superintendent, that a large piping condition had <br />been discovered near the north end of the east embankment in which <br />approximately 400 gpm of muddy flow was exiting beyond the toe of <br />the downstream slope into the West Ditch. I arrived at the site at <br />approximately 4:15 P,M, and found the condition to be as described. <br />A piping hole of approximately 18 inches in diameter was visible in <br />the west slope of the West Ditch, approximately 5 feet below the <br />top of the ditch. A second smaller pipe and seep was visible <br />approximately 20 feet to the north. This flow was not nearly as <br />muddy and flow was estimated at 40 to 50 gpm, A captured flow <br />sample in a one gallon bucket from the large pipe was allowed to <br />decant and approximately 1 inch of sediment was visible in the <br />bottom of the bucket. A large crack and saturated slide was visible <br />along the West Ditch, adjacent to the piping location, <br /> <br />The reservoir was at gage height 10 feet, which is full, Allen had <br />ceased diverting into the reservoir and had begun releasing at a <br />rate of approximately 125 cfs, the outlet channel capacity, It was <br />determined that at this rate, it would take nearly two weeks to <br />lower the reservoir down to the seepage level, <br />-1-0 <br />In an effort^ slow down the erosive flow which was occurring, a <br />large front end loader with a full bucket of sand was used to roll <br />over and collapse the smaller pipe to the north, A cavern was <br />exposed in which flowing water was clearly visible, Several loader <br />buckets of sand were placed in the cavern and the flow was <br />completely stopped. After the successful attempt on the smaller <br />pipe, the same procedure was used on the larger pipe and by <br />approximately 8:30 P.M., the flow from the large pipe was reduced <br />to less than 1 gpm and flowing clear. <br /> <br />It is believed that a sand lens in the embankment cross section is <br />the source of the seepage and piping and that the seepage may have <br />followed a rodent hole into the West Ditch. The reservoir will <br />continue to be drawn down to gage height 7 feet and the possibility <br />of using sheet piling to cut off the seepage flow from the sand <br />lens is currently being evaluated by the owner's engineer, Robert <br />M, Robler. The owner will continue to monitor the condition <br />closely. <br /> <br />Michael L. Graber <br />Division 2 Dam Safety Engineer <br /> <br />xc: Alan Pearson, Allen Ringle, Don Taylor <br />
The URL can be used to link to this page
Your browser does not support the video tag.