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PROJ00137
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PROJ00137
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Last modified
11/19/2009 11:43:09 AM
Creation date
10/5/2006 11:38:26 PM
Metadata
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Template:
Loan Projects
Contract/PO #
C153467
Contractor Name
Greeley, City of
Contract Type
Loan
Water District
0
County
Weld
Bill Number
XB 99-999
Loan Projects - Doc Type
Feasibility Study
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<br />I <br />I <br />1 <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />1 <br />I <br />I <br />I <br />I <br />I <br />I <br /> <br />internal fri cti on for the dam material of 35 to 40 degrees, wi th mi nimal <br />cohesion. The coefficient of permeability of a typical embankment sample was <br />5 x 10-5 cm/see., consi stent with the results of the fi el d permeabi li ty <br />tests. <br /> <br />Potential RCC aggregate included materials comprising the existing dam and <br />upper reservoi r gl aci a 1 till deposi ts. A set of six RCC test cyl i nders were <br />cast from unprocessed embankment materi al s (test pit TLP-51, using a cement <br />content of 150 1 b/cy. Compressi ve strength tests were scheduled for 7; 28, <br />and 56 days. Strength results were poor, and subsequent testing of the <br />aggregates for Los Angel es abrasi on wear and sodi um sulfate soundness loss, <br />yielded values unacceptable for RCC. The high percentages of weak particles <br />and micaceous mineral s in the weathered rock was probably responsible for the <br />poor results. The glacial till deposits from the upper reservoir area consist <br />of more durable transported sands and gravel s. However, insufficient sample <br />volume was obtained from TLP-2 to allow for aggregate testing in the <br />1 aboratory. <br /> <br />Materi al from TLP-8 was assi gned a borderl i ne cl assifi cati on of si 1 t to 1 ean <br />-6 <br />cl ay (Ml-CLl, wi th a coeffi ci ent of permeabil ity of 2 x 10 cm/sec. The <br />material could be utilized for an impervious zone, but available quantities <br />are questionable. <br /> <br />Further detail s on 1 aboratory test results for soil sampl es from Twi n Lakes <br />Oam and Reservoir are included in Appendix C. <br /> <br />2.3 Slope Stability of Existing Dam <br /> <br />2.3.1 Procedure <br /> <br />Static stabil i ty analyses of the exi sti ng embankment were performed usi ng the <br />Modified Bishop limit equilibrium procedure. Two different embankment loading <br />conditions were analyzed. These loading conditions were: <br /> <br />-50- <br />
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