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Last modified
1/25/2010 7:15:07 PM
Creation date
10/5/2006 3:46:10 AM
Metadata
Fields
Template:
Floodplain Documents
County
Costilla
Community
San Luis
Stream Name
San Luis area drainageway
Basin
Rio Grande
Title
Master Drainage Study Town of San Luis
Date
12/1/1988
Prepared For
San Luis
Prepared By
WRC Engineering, Inc.
Floodplain - Doc Type
Floodplain Report/Masterplan
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<br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br />I <br /> <br />difference in the water level. Valley Pump increased the pumping <br />rate to 22 gpm and the test wells were monitored again for 15 <br />minutes with no change in the water level. At this point WRC <br />determined that the pumping test was not yielding conclusive <br />results, so pumping was discontinued. <br /> <br />Due to the failure of the pumping test to yield positive results, it <br />was necessary to estimate the properti es of the aqui fer by other <br />methods. Sieve analysis was performed on soil samples from 4 of the <br />test well s and an average permeabil ity of 106 gpd/ft2 was <br />determined. Based on a length of 1200 feet (the maximum width of <br />the three block area in the northeast part of town) and lowering the <br />water table by a maximum of 4 feet, the interception rate required <br />woul d be 0.73 cfs. Thi s is the mi nimum rate that the dewateri ng <br />system will be based on. <br /> <br />3. <br /> <br />Alternative Solutions <br /> <br />, -' <br /> <br />Two different means of lowering the water table were investigated: <br />a) system of well poi nts and b L subdrai n perforated pi pe system. <br />The investigation considered the engineering and construction <br />concepts as well as installation plus operation and maintenance <br />costs in developing the project recommendation. <br /> <br />a. Well Points <br /> <br />WRC determined that in order to drop the water table a depth of <br />two feet using well points would require approximately 60 well <br />points along (spaced at 20' along a 1200' line). The initial <br />cost of this system is estimated to be from $50,000 to $70,000. <br />O&M costs per year were estimated at $50,000 a year, including <br />pump rental and normal maintenance. <br /> <br />b. Subdrain system (gravity flow) <br /> <br />A gravity subdrain <br />east-west perforated <br /> <br />system consisting of three parallel <br />pipes connected to a sol id north-south <br /> <br />-15- <br />
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